Aviation Accident Summaries

Aviation Accident Summary LAX99LA081

LEMOORE, CA, USA

Aircraft #1

N67064

Hiller UH-12E

Analysis

While maneuvering during an aerial application flight at 15 feet above an alfalfa field, the pilot heard a noise emanating from the engine, and it seized. The pilot made a forced landing in the underlying soft field, and the helicopter rolled over after touching down on the uneven terrain. Maintenance records review disclosed that the helicopter's engine had operated about 482 hours since being overhauled. The engine examination revealed that the number two connecting rod was broken at its crankshaft end. Additionally, an inspection of the associated cylinder and piston revealed evidence of detonation. Similar excessive heat exposure signatures were observed with the other five piston heads. A small hole was found chaffed into the fuel primer line. Carbon deposits and burned rotor fingers were found in both magnetos.

Factual Information

On January 24, 1999, about 0900 hours Pacific standard time, a Hiller UH-12E, N67064, operated by Breen Aviation, Inc., experienced a total loss of engine power while maneuvering during an aerial application flight about 7 miles north of Lemoore, California. The flight was being conducted under the provisions of 14 CFR Part 137. The pilot reported that he heard a noise emanating from the engine. Thereafter the engine seized, and the pilot stated he made a forced landing from his altitude of 15 feet above ground level. Following touchdown in the soft, uneven alfalfa field, the helicopter rolled over and was substantially damaged. The commercial pilot was not injured. Visual meteorological conditions prevailed, and no flight plan was filed. The flight originated from a nearby field about 0800. The helicopter was recovered and examined by Federal Aviation Administration (FAA) airworthiness inspectors from the Fresno, California, Flight Standards District Office. Maintenance records indicated that the helicopter's engine had been operated about 482 hours since being overhauled. The FAA inspectors reported that the engine's number two connecting rod was found broken at its crankshaft end, and the break did not appear related to the rod bolts. Additionally, an inspection of the associated cylinder and piston showed signatures consistent with detonation. Similar signatures indicative of exposure to elevated temperatures were observed with the other five piston heads. Maintenance discrepancies were also noted with the primer line and magnetos. A small hole was found chaffed in the primer line. The magneto distributor blocks for both magnetos showed evidence of carbon and burning of the rotor fingers. The magnetos were subsequently bench tested and were found functional.

Probable Cause and Findings

The inadequate nature of the operator's maintenance, which failed to detect the primer and magneto discrepancies. An overly lean fuel mixture and/or magneto cross firing resulted in detonation, an ensuing connecting rod failure, and a total loss of engine power. Contributing factors were the helicopter's low altitude and the uneven, soft nature of the terrain.

 

Source: NTSB Aviation Accident Database

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