Aviation Accident Summaries

Aviation Accident Summary FTW94LA089

GALLUP, NM, USA

Aircraft #1

N201SX

MOONEY M20J

Analysis

AT 8,500 FEET MSL THE PILOT EXPERIENCED A LOSS OF ENGINE POWER DUE TO THE FAILURE OF THE EXHAUST VALVE FOR THE NUMBER THREE CYLINDER. THE PILOT ATTEMPTED A FORCED LANDING TO A SNOW COVERED OPEN FIELD. DURING THE LANDING ROLL, THE RIGHT MAIN LANDING GEAR COLLAPSED AFTER IMPACTING A TREE STUMP.

Factual Information

On February 24, 1994 at 0942 mountain standard time, a Mooney M20J, N201SX, was substantially damaged during a forced landing near Gallup, New Mexico. The private pilot was not injured. Visual meteorological conditions prevailed for the personal flight. The pilot stated in the enclosed pilot/operator report that while in cruise flight at 8,500 feet MSL, he heard a "pop-like" sound coming from the engine, immediately followed by a severe engine vibration. The pilot added that the engine lost power and he proceeded to shut down the engine. A forced landing to a snow covered open field was performed. The pilot elected to land with the landing gear extended. During the landing roll the right main landing gear collapsed after it collided with tree stump. Post accident examination of the engine revealed that the exhaust valve for the number 3 cylinder failed, resulting in the total loss of engine power.

Probable Cause and Findings

THE LOSS OF ENGINE POWER DUE TO THE FAILURE OF THE NUMBER 3 EXHAUST VALVE. A FACTOR WAS THE LACK OF SUITABLE TERRAIN AVAILABLE TO EXECUTE THE FORCED LANDING.

 

Source: NTSB Aviation Accident Database

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