Aviation Accident Summaries

Aviation Accident Summary CHI94LA249

WATERFORD, MI, USA

Aircraft #1

N93572

BELLANCA 17-30

Analysis

ON INITIAL VFR CLIMBOUT THE ENGINE RAN ROUGH THEN LOST POWER. THE PILOT REPORTED THAT DURING THE DESCENT HE ATTEMPTED TO SWITCH FUEL TANKS BUT DOES NOT REMEMBER HIS EXACT PROCEDURES. THE AIRPLANE IMPACTED IN A LAKE. POST ACCIDENT EXAMINATION REVEALED THE FUEL SELECTOR VALVE SET TO AN INTERMEDIATE POSITION BETWEEN THE LEFT AND RIGHT FUEL TANKS, AND ONLY A FEW TEASPOONS OF FUEL IN THE FUEL LINES BETWEEN THE FUEL SELECTOR VALVE AND THE FUEL INJECTOR NOZZLES. ALL ACCESSORIES OPERATED NORMALLY AND THE ENGINE RAN ON A TEST STAND.

Factual Information

On July 29, 1994, at 0921 hours central daylight time, a Bellanca BL-17-30, N93572, operated as a personal aircraft by Wooden Airplane Company of Southfield, Michigan, impacted water in a lake in Waterford, Michigan. The airplane was substantially damaged, the private pilot and two passengers sustained serious injuries. Visual meteorological conditions existed at the time of the accident. The airplane was departing on an instrument flight plan to Oshkosh, Wisconsin, and impacted one half mile west of the departure end of runway 27R from Oakland-Pontiac Airport, Pontiac, Michigan. The pilot reported that during the initial climbout the engine began to run rough and lost power. He reported attempting to switch fuel tanks, but could not remember his exact actions. The impact ruptured both wing fuel cells. The fuel lines to the engine remained intact. Postaccident examination revealed less than 1 ounce of fuel in the fuel lines from the selector valve to the strainer, and the strainer to the engine driven and electric pumps. An internal examination of the fuel selector valve revealed that the port from the right tank was half open. Both pumps were bench operated and discharged fuel once primed. Inspection of the magnetos, plugs, and induction system revealed no discrepancies. The propeller was pulled through and the accessories turned with no binding. The engine was run on a test stand with normal magneto checks and the propeller responded normally to the pitch control. The engine was run up to 1600 RPM with no anomalies. At that point acceleration was stopped due to vibration from bent propeller blades. Shut down was normal using the mixture control.

Probable Cause and Findings

undetermined.

 

Source: NTSB Aviation Accident Database

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