Aviation Accident Summaries

Aviation Accident Summary CHI95LA058

MINNEAPOLIS, MN, USA

Aircraft #1

N3983H

MOONEY M20K

Analysis

THE PILOT STATED THAT AFTER TAKEOFF AT AN ALTITUDE OF 200 FEET AGL, THE ENGINE BEGAN RUNNING ROUGH AND LOST POWER. HE DECLARED AN EMERGENCY AND WAS INITIALLY CLEARED TO LAND ON RUNWAY 23R FOLLOWED BY A CLEARANCE TO LAND ON ANY RUNWAY. HE STATED HE DID NOT INITIALLY UNDERSTAND THAT HE WAS CLEARED FOR ANY RUNWAY SO HE SET UP TO LAND ON RUNWAY 23R. HE STATED HE WAS TOO CLOSE TO THE RUNWAY BUT HE CONTINUED THE LANDING. THE AIRPLANE TRAVELED OFF THE END OF THE RUNWAY AND CAME TO A STOP AFTER CONTACTING AN AIRPORT PERIMETER FENCE. A POST ACCIDENT TEST RUN OF THE ENGINE REVEALED IT PRODUCED POWER TO 2700 RPM. THE ONLY ANOMALY FOUND WAS A SEPARATION OF THE #6 CYLINDER EXHAUST PIPE NEAR ITS ENGINE MOUNTING FLANGE.

Factual Information

On December 28, 1994, about 1517 central standard time, a Mooney M20K, N3983H, sustained substantial damage in a precautionary landing at the Crystal Airport, Minneapolis, Minnesota, when it departed the end of runway 23R, and struck the airport perimeter fence. Neither the commercial pilot, nor the single passenger aboard the airplane were injured. The flight had just departed the Crystal Airport with an intended destination of Rockford, Illinois. An IFR flight plan was filed, and visual meteorological conditions prevailed at the time. The pilot stated that at an altitude of approximately 200 feet agl, after takeoff, the engine started running rough and an "significant loss of power" occurred. The pilot declared and emergency and was cleared to land on runway 23R. The pilot was later cleared to land on any runway. The pilot stated he, "Did not fully realize all runway[s] were available." He set up for a landing on runway 23R. He stated he was not set up properly, being too close, but decided to land anyway. The airplane touched down long on the runway, traveled off the end and contacted an airport perimeter fence. A post accident engine test run was conducted. The engine ran up to 2700 rpm without interruption. The only anomaly noted on the was that the #6 cylinder exhaust pipe had separated near the mounting flange.

Probable Cause and Findings

the pilot's misjudging of distance and airspeed during the approach to landing which resulted in an overrun. Factors associated with the accident were the separation of the exhaust pipe and the pilot's not understanding communications from the air traffic control tower.

 

Source: NTSB Aviation Accident Database

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