Aviation Accident Summaries

Aviation Accident Summary FTW95LA117

PLANO, TX, USA

Aircraft #1

N5096U

CESSNA 172RG

Analysis

WHILE DESCENDING EN ROUTE, THE ENGINE LOST POWER AND A FORCED LANDING WAS MADE IN A PLOWED FIELD. THE NOSE WHEEL SEPARATED AND THE AIRPLANE NOSED OVER COMING TO REST INVERTED. DISASSEMBLY OF THE ENGINE REVEALED A LOSS OF GEAR TRAIN CONTINUITY DUE TO THE LOOSENING OF THE CRANKSHAFT GEAR RETAINING BOLT AND THE SUBSEQUENT FRACTURE OF THE CRANKSHAFT GEAR ALIGNMENT DOWEL. THE AIRPLANE'S PROPELLER HAD BEEN REPLACED ON 02/13/92 FOLLOWING A NOSE GEAR COLLAPSE; HOWEVER, AD 91-14-22 WAS NOT COMPLIED WITH AS THE ENGINE DID NOT EXPERIENCE SUDDEN STOPPAGE.

Factual Information

On February 17, 1995, at 1235 central standard time, a Cessna 172RG, N5096U, was substantially damaged during a forced landing near Plano, Texas. The commercial pilot and his passenger were not injured. Visual meteorological conditions prevailed for the repositioning flight from McKinney, Texas, to Addison, Texas. The airplane was in a descent 7 miles northeast of Addison Airport when the engine lost power. After attempting unsuccessfully to restart the engine, the pilot landed in a plowed field. According to the pilot, when the nose wheel touched down in the soft dirt it "dug in and broke off" and the "airplane performed a forward somersault and came to rest inverted." A Federal Aviation Administration inspector reported that the right wing spar was bent and the upper portions of the vertical stabilizer and rudder were crushed. Examination and disassembly of the engine on 03/06/95 revealed a lack of gear train continuity. The crankshaft gear lockplate tang was sheared and the crankshaft gear retaining bolt had backed out of the crankshaft to the point where no threads were engaged. The crankshaft gear alignment dowel was fractured. An examination of the aircraft logbooks by a Federal Aviation Administration inspector revealed that the propeller had been replaced on 02/13/92 following a nose gear collapse. Airworthiness Directive (AD) 91-14-22 was not complied with at that time. The AD requires an inspection of the crankshaft gear following any propeller strike which results in sudden engine stoppage. According to the operator, the nose gear collapse did not result in sudden engine stoppage.

Probable Cause and Findings

THE DISENGAGEMENT OF THE CRANKSHAFT GEAR DUE TO THE LOOSENING OF THE GEAR RETAINING BOLT AND THE SUBSEQUENT FRACTURE OF THE GEAR ALIGNMENT DOWEL. A FACTOR WAS THE LACK OF SUITABLE TERRAIN AVAILABLE FOR THE FORCED LANDING.

 

Source: NTSB Aviation Accident Database

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