Aviation Accident Summaries

Aviation Accident Summary LAX95LA178

PHOENIX, AZ, USA

Aircraft #1

N4357Q

GODKEY KITFOX IV

Analysis

THE AIRCRAFT WAS IN THE TAKEOFF INITIAL CLIMB WHEN THE PILOT DECLARED AN EMERGENCY. THE AIRCRAFT COMPLETED A TURN BACK TOWARD THE RUNWAY, LANDED SHORT OF THE AIRPORT BOUNDARY, AND STRUCK THE PERIMETER FENCE. THE PILOT REPORTED THAT HE HAD JUST TAKEN OFF WHEN HE NOTICED THAT THE ENGINE WAS NOT DEVELOPING FULL POWER. JUST THEN, THE ENGINE QUIT. HE ATTEMPTED TO TURN BACK TOWARD THE RUNWAY BUT DID NOT HAVE SUFFICIENT ALTITUDE TO REACH THE RUNWAY. A POSTACCIDENT INSPECTION REVEALED THAT THE IGNITION SYSTEM WAS INOPERATIVE DUE TO A DEFECTIVE DIODE.

Factual Information

On May 3, 1995, at 0735 mountain standard time, a homebuilt Godkey Kitfox IV, N4357Q, sustained substantial damage during a forced landing at Phoenix, Arizona. The aircraft was owned and operated by the student pilot and was on a local instructional flight. Visual meteorological conditions prevailed and no flight plan was filed. Neither the certificated flight instructor nor the student were injured. The flight originated from the Phoenix-Deer Valley Municipal Airport at 0730 on the day of the accident. The tower operator had just cleared the aircraft for takeoff from runway 25L when she heard the pilot declare an emergency. Looking in the direction of departure, she saw the aircraft complete a 180-degree turn back toward the runway. As she continued watching, the aircraft landed short of the airport boundary and struck the perimeter fence. The instructor reported that the aircraft had just taken off on runway 25L when the student, who was on the controls, informed him that the engine tachometer was not indicating full power. Just as he made the statement, the engine quit. He attempted a left 180-degree turn back toward the departure runway but did not have sufficient altitude to reach the runway and was forced to land short. A postaccident inspection by an Federal Aviation Administration (FAA) airworthiness inspector revealed that the ignition system was inoperative due to a defective diode. Spark plugs were inspected for serviceability and wiring was checked for continuity.

Probable Cause and Findings

the failure of the ignition system due to a deffective diode.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports