Aviation Accident Summaries

Aviation Accident Summary CHI95LA291

MIO, MI, USA

Aircraft #1

N76429

CESSNA 140

Analysis

The airplane departed runway 27 and obtained about 10 to 30 feet of vertical clearance with the trees at the end of the airport property. It went into a 60 to 90 degrees angle of bank to the left and leveled out for about 1/4 mile. The airplane went into another ninety degree left bank. The airplane hit trees with the left wing pointing down and landed in an inverted position. Witnesses reported the engine had sounded normal with no sputtering during the flight. Examination of the engine and aircraft failed to reveal any anomalies. The reported local winds were 270 degrees at 11 miles per hour, gusting to 20. The toxicology examination indicated that Chlorpheniramine (0.136 ug/ml) was detected in the blood. This drug is not approved for use while piloting an airplane. Chlorpheniramine is an ingredient in Contact. A witness reported that the pilot had not been feeling well, and that the pilot was lethargic and was just in 'slow motion.' The witness reported that the pilot took one Contact in the morning.

Factual Information

History of Flight On August 21, 1995, at 1253 eastern daylight time, a Cessna 140, N76429, was destroyed as a result of loss of control while maneuvering after takeoff. The private pilot was fatally injured. The 14 CFR Part 91 flight departed the Oscoda County Airport, Mio, Michigan, en route to Marine City, Michigan. Visual meteorological conditions prevailed and no flight plan was filed. Witnesses reported that the pilot departed from runway 27 at Oscoda County Airport. The takeoff was normal and the engine sounded normal with no sputtering. Shortly after takeoff the pilot rocked his wings as a goodbye gesture, which was typical for the pilot. Witnesses reported that the airplane obtained about 10 to 30 feet of vertical clearance with the trees at the end of the airport property. The airplane went into a hard bank to the left, which was reported to be between 60 to 90 degrees angle of bank. The airplane crossed highway 33 during the turn and leveled out for about 1/4 mile. A witness driving south on highway 33 reported that he could see the airplane out the right side of his pickup window. He reported that the airplane was no more than 20 feet above the trees. The airplane went into another hard, ninety degree left bank which turned the aircraft back toward the airport property heading about 120 degrees. Witnesses reported that the airplane hit trees with the left wing pointing down. The airplane landed in an inverted position. Witnesses also reported that the engine had sounded normal with no sputtering during the flight. Personnel Information The pilot was a 49 year old male, private pilot. He had flown his biennial flight review 26 months prior in a Cessna 140. He held a second class medical certificate and the date of his last medical exam was August 15, 1994. He had flown 625 total flight hours. He had logged 3 hours of flight time in the last 90 days. Aircraft Information The airplane was 1946 Cessna 140 and was owned by the pilot. The aircraft's logbooks were not recovered. The last recorded annual inspection was performed on April 26, 1994, and the total hours on the airplane were 2,940 hours. The tach time at the accident site indicated 3,153 total hours. Witnesses reported that the pilot had purchased five gallons of automobile fuel the morning of the accident to be used in his airplane. Wreckage and Impact Damage An Airworthiness Inspector from the Federal Aviation Administration reported that the wreckage path indicated the airplane impacted the trees with the left wing down and then rolled inverted and struck the ground. He reported that the engine went into the cabin when the nose hit the ground. He reported that there were indications of propeller strikes in the trees. The inspector reported that engine was operating at the time of the accident, and that the engine and flight controls had continuity. Meteorological Conditions Visual meteorological conditions prevailed at the time of the accident. The reported local winds were 270 degrees at 11 miles per hour, gusting to 20 miles per hour. Witnesses reported winds had been between 20 and 40 miles per hour that day. Medical and Pathological Information The autopsy was performed at Mercy Hospital/Grayling, 1100 Michigan Ave., Grayling, MI 49738. The toxicology report indicated the following results: 0.136 (ug/ml, ug/g) Chlorpheniramine detected in Blood Phenylpropanolamine was detected in Blood Atropine was detected in Blood Use of Chlorpheniramine is not approved for use while piloting an airplane. Chlorpheniramine is an ingredient in Contact. A witness reported that the pilot had not been feeling well during the weekend. The witness reported that the pilot had not been himself and was "kind of doggy" all morning. The witness reported that the pilot was lethargic, and that he could not keep his eyes open and was just in "slow motion." The witness reported that the pilot took one Contact in the morning for his allergies and hay fever. Additional Information Parties to the investigation included Cessna Aircraft Company and the Federal Aviation Administration. The airplane wreckage was released to the family.

Probable Cause and Findings

the pilot's impairment of judgement and performance which led to performing a low altitude maneuver with insufficient altitude for recovery. A factor was the tailwind.

 

Source: NTSB Aviation Accident Database

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