Aviation Accident Summaries

Aviation Accident Summary CHI96LA076

CHESTERFIELD, MO, USA

Aircraft #1

N24311

Cessna 152

Analysis

The student pilot reported that he was on his first unsupervised solo, and was practicing touch-and-go's. On the first landing he hit hard and began to porpoise. He tried to set an approach attitude after the third bounce, but lost directional control on the ground. The airplane was heading for a row of hangars so he attempted to takeoff, but was unable to clear the hangars. The airplane struck the hangars at the roof line and came to a stop. The student pilot's instructor reported that instruction concerning porpoising had been discussed. The student pilot recalled that he had received instruction about porpoising, but it had not been discussed in detail. He had been told to set an approach attitude, but was uncertain exactly what that meant. Parts of the wheel rim were found on the runway.

Factual Information

On January 14, 1996, at 0935 central standard time, a Cessna 152, N24311, operated by Phoenix Aviation, Chesterfield, Missouri, sustained substantial damage when it impacted and remained on the roof of a hangar after an aborted landing. The student pilot received minor injuries. The 14 CFR Part 91 flight departed the Spirit of St. Louis Airport, Chesterfield, Missouri, on a local student flight. Visual meteorological conditions prevailed and no flight plan was filed. The student pilot reported that he planned to practice touch and go's during the flight. On the first landing he hit hard and bounced. The airplane landed on the nose wheel and started porpoising. He reported that he tried to recover after the third bounce by setting an approach attitude, but lost directional control. The airplane veered off runway 26R to the left 90 degrees, and was heading for a row of hangars. He applied full throttle and tried to gain enough altitude to clear the hangars. The airplane impacted the hangar at the roof line and came to a stop. The pilot secured the airplane, and with help from others, was able to climb down to safety. An Operations Inspector from the Federal Aviation Administration reported that the student pilot was on his first unsupervised solo. He reported that the skid marks on the ground revealed that the airplane veered off the runway and was still on the ground as it headed for the hangars. He also reported that parts of the wheel rim had broken off during the impact and been found on the runway. The Operations Inspector asked the student pilot's flight instructor about the student pilot's flight proficiency. The instructor characterized the student pilot as a "great student" who was quick to learn and apply new knowledge. Asked whether recovery from a porpoising situation had been covered during their instruction, the instructor responded that the situation had been discussed. When the student pilot was questioned about instruction he had received concerning porpoising, he recalled it had been discussed, but not in detail. The student pilot reported that the instructor had told him to re-establish the approach attitude, but he was uncertain exactly what that meant.

Probable Cause and Findings

the pilot misjudged the flare and performed an improper recovery from a bounced landing. A factor was the inadequate ground instruction concerning recovery from a bounced landing.

 

Source: NTSB Aviation Accident Database

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