Aviation Accident Summaries

Aviation Accident Summary CHI96LA093

WORTHINGTON, MN, USA

Aircraft #1

N758CQ

CESSNA 172

Analysis

After climbing to 3500 feet, the pilot noted that smoke was entering the cockpit and that the engine was beginning to run rough. He diverted back toward the airport, but noted that the oil pressure began dropping rapidly and that the RPM began to fluctuate. The pilot then decided to secured the engine and make an emergency landing on a gravel road. During the landing, the right wing hit a yield sign on the side of the road. There was no indication of oil on the dipstick. A two to three inch hole was discovered in the crankcase of the engine. Examination of the engine revealed that a hole had been burned through the number three piston; the #1 and #2 connecting rods were off the crankshaft; and the #1 and #2 crankshaft journals were partially melted. The fuel system was checked and no defects were discovered. An examination of the magnetos revealed that the race inside the left magneto was loose and rotating within the aluminum housing. Metal particles from the race and housing covered the surface around the magneto block.

Factual Information

On February 18, 1996, at 1310 central standard time, a Cessna 172, N758CQ, sustained substantial damage during a forced landing due to loss of engine power near Worthington, Minnesota. The private pilot and two passengers reported no injuries. The 14 CFR Part 91 flight departed Worthington Municipal Airport, Worthington, Minnesota, at 1255 cst, en route to Buffalo Municipal Airport, Buffalo, Minnesota. Visual meteorological conditions prevailed and no flight plan was filed. The pilot reported that he departed Worthington, Minnesota, and climbed to 3,500 feet. The first indication that something was wrong was the engine began running rough and there was light smoke in the cockpit. The pilot reported that all the instruments were in the green, the power was set at 2500 RPM with 23 inches of manifold pressure, and the mixture was at full rich. He noticed the oil pressure decreasing and he turned back to land at Worthington Airport. He reported that the engine RPM's began fluctuating, the oil pressure dropped rapidly, and the cockpit began filling with smoke. The pilot decided to secure the engine and execute a forced landing to a gravel road. The airplane touched down on the road, but during landing rollout the right wing hit a yield sign on the side of the road. The airplane swerved into an adjacent field and came to a complete stop. The oil was checked and there was no indication of oil on the dipstick. A two to three inch hole was discovered in the crankcase of the engine. An examination of the engine revealed that the number three piston exhibited a hole burned in the bottom side through the crown structure to the piston interior. The number one and number two connecting rods were off the crankshaft. The connecting rod bolts were broken. The bolts were black and necked down at the fractured area. The number one and two crankshaft journals were partially melted. The number three, four, and five connecting rods were burned and discolored. The crankshaft main bearings exhibited normal operational signatures. The fuel system was checked and no defects were discovered. An examination of the magnetos revealed that the left magneto was contaminated with a blackish debris. The left magneto distributor block interior was coated with the debris. The rear bearing race was found spinning in the left magneto's aluminum housing. Metal particles from the race and housing covered the surface around the magneto distributor block.

Probable Cause and Findings

Progressive failure of the engine, beginning with failure of the left magneto, which resulted in preignition or detonation, a burned hole in the #3 piston, subsequent oil exhaustion, and failure of the #1 and #2 connecting rods.

 

Source: NTSB Aviation Accident Database

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