Aviation Accident Summaries

Aviation Accident Summary IAD96IA098

JAMAICA, NY, USA

Aircraft #1

N606FF

Boeing 747-136

Analysis

The pilots stated that at flight level 350, just before their descent to JFK, the No. 2 engine generator warning light and CSD low oil pressure light illuminated. Attempts to disconnect the CSD were unsuccessful, and the No. 2 engine was shut down. Following the shutdown, the No. 2 engine fire warning sounded, and the flightcrew discharged both No. 2 engine fire bottles; however, the fire continued. After declaring an emergency and landing at JFK, firefighters noted that the gearbox was glowing red, and they used extinguishing agent. Examination of the engine and accessory gearbox components revealed that the CSD failed to disconnect, because it had not been overhauled in accordance with the manufacturers overhaul manual.

Factual Information

HISTORY OF FLIGHT On June 17, 1996, at about 2130 eastern daylight time (EDT), a Boeing 747-136, N606FF, operated by Tower Air, Inc., as Flight 22, sustained minor damage when the Number 2 engine fire warning light illuminated at an altitude of 35,000 feet mean sea level, during the aircraft's arrival/descent into the John F. Kennedy (JFK) International Airport, in Jamaica, New York. The crew shut down the engine, and discharged both engine fire extinguishing bottles. The flight crew declared an emergency and landed at JFK on runway 31L, without further incident. There were no reported injuries among the 17 crewmembers and 397 passengers who were deplaned from the right side of the aircraft using mobile stairs. The flight originated from Los Angeles International Airport (LAX), at 1644 EDT. Visual meteorological conditions prevailed, and an Instrument Flight Rules (IFR) flight plan had been filed. The flight was conducted under the provisions of Title 14 Code of Federal Regulations (CFR) Part 121 as a domestic, scheduled passenger flight. The pilots said that at flight level 350, just before the top of their descent into JFK at about 2055, the No. 2 engine generator (GEN) warning light and constant speed drive (CSD) low oil pressure light illuminated indicating a problem with both the GEN and CSD. The flight engineer selected and tested the GEN and CSD, and found that the CSD oil temperature was high, at over 150 degrees Celsius, and the GEN kilowatt output was low, at -20 kilowatts. The flight engineer stated that he attempted to disconnect the CSD but was unsuccessful. At 2100, the No. 2 engine was shut down. The captain contacted the purser/lead flight attendant and briefed her on the situation and instructed her to inform her crew and review evacuation procedures. Moments later the fire warning sounded, and the flightcrew discharged both No. 2 engine fire bottles; however, the fire continued. Airport Rescue and Fire Fighting (ARFF) personnel were standing by and foamed the engine when the aircraft came to a complete stop. According to firefighters, the magnesium gearbox was glowing red when the aircraft landed and they had to extinguish it with foam. WRECKAGE EXAMINATION/DOCUMENTATION On June 20, 1996, the National Transportation Safety Board examined the engine that had caught on fire and found that the fire had originated in the engine's accessory gearbox. The engine cowling adjacent to the gearbox had sustained substantial fire damage, including scorching, soot, and burn through. Examination of the gearbox revealed that the magnesium casing adjacent to the GEN had burned/melted away, exposing the internal gears of the gearbox. Examination of the CSD and GEN, which were connected on opposite sides of the gearbox and to each other through the use of a "transfer tube," found that the input quill shaft on the generator had separated near the base of the generator. Examination of the aircraft's electrical system found electrical continuity between the disconnect switch in the cockpit and the CSD disconnect solenoid. Because the CSD failed to disconnect, the unit was sent to Sundstrand Aerospace, the manufacturer of the CSD, for further examination. On July 23, 1996, personnel from the Safety Board, Tower Air, Boeing Commercial Airplane Group, Federal Aviation Administration (FAA), and Sundstrand examined the unit. During the external examination, it was noted that the CSD unit had been overhauled by UNC Accessory Services at its Fort Lauderdale, Florida, facility in December 1994, and returned to Tower Air in January 1995. According to Tower Air personnel, at the time of the incident on June 17, 1996, the unit had accumulated 3,758 hours since overhaul. Upon disassembly of the unit, examination of the electrical wiring harness and subsequent tests of the disconnect solenoid found that it functioned, in all modes including high temperatures and low voltage. However, internal examination of the CSD unit revealed that the mounting screws had loosened on the output gear bearing support, governor bearing support, and charge pump. Three of the four screws installed in the bearing support for the output gear had completely backed out of the output housing support mounts. The remaining screw had partially backed out but was contained in the bearing support screw hole by surrounding hardware. Additionally, some of the screws used were shorter than those specified in Sundstrand's 6OAGD09 Overhaul Manual 24-11-00. (See attached photographs.) Tower Air provided the Board with another CSD that had been overhauled by UNC's Fort Lauderdale facility, which personnel from the Safety Board, Tower Air, FAA, and Sundstrand examined on July 30, 1996. It was noted during the external examination that the unit had been overhauled in December 1993 and returned to Tower Air in January 1994. Tower Air reported that at the time of the July 30, 1996, examination, the unit was airworthy and had accumulated 4,436 hours since overhaul. While disassembling the unit, investigators noted that the end cover was attached with five screws, four of which were shorter than those specified in Sundstrand's overhaul manual. In addition, internal examination revealed that safety wire was used to secure the bearing support mounting screws, the scavenge pump mounting screws, and the governor trim head to the governor support mounting screws. Those screws that were not safety wired had a liquid fastener applied to help secure them where no liquid fastener was called for in the overhaul manual. Additionally, according to Sundstrand personnel the self-locking helicoils that were used no longer retained their self-locking capability. Sundstrand's overhaul manual specifically explained into which screw plates the screws were to go. The Sundstrand Standard Practices Manual 24-10-00 also addressed the use and test procedures for self-locking helicoils. The manuals did not mention the use of safety wire on the above-mentioned components. According to Sundstrand, it does not use or recommend safety wire during the internal assembly processes of the CSD. The Sundstrand Constant Speed Drive Design Guidebook specifies to avoid the use of safety wire to lock screws, especially inside the unit. An exception is the hydraulic unit fixed-slipper retainer wedge retaining screws. According to Sundstrand personnel, Sundstrand avoids the use of safety wire because of concerns about contamination inside the unit, and the difficulty of safety wiring within the confines of the CSD housing. Sundstrand stated that the only internal CSD component in which safety wire is utilized is the hydraulic log unit. The retaining screws within the hydraulic log are safety wired in place because self-locking helicoil inserts cannot be used in that location. Further, this is done as a component assembly process outside of the CSD housing, eliminating internal contamination concerns. On August 6, 1996, the Safety Board examined the FAA's principal maintenance inspector's (PMI) inspection records for UNC's Fort Lauderdale facility. The records indicated that from June 3 to June 7, 1991, the FAA's Fort Lauderdale Flight Standards District Office (FSDO) conducted an in-depth inspection of UNC's Fort Lauderdale facility. One of the findings from the inspection was that the facility was not reporting malfunctions or defects as required by 14 CFR Part 145.63(a). As a result of this finding, UNC's Fort Lauderdale facility incorporated acceptable procedures into its inspection procedures manual. According to the FSDO Office Manager, the PMI who had been assigned to UNC's Fort Lauderdale facility for the last 2 years had conducted two inspections of the facility both within the last year. Both inspections found discrepancies with the facility's inspection procedures manual similar to those found in the FSDO inspection conducted in 1991. On August 7, 1996, the Safety Board examined UNC's Fort Lauderdale facility. The examination revealed that the facility did not record Malfunction Defect Reports (SDR) in accordance with its inspection procedures manual or 14 CFR Part 145.63(a). Also, teardown reports were not fully completed on the two CSD's provided by Tower Air for this investigation as required by UNC's Fort Lauderdale facility inspection procedures manual, there were no test specifications found for the incident CSD to return it to service after overhaul, and dimensional checks of internal components were completed with no indication about who performed the checks or what the actual dimensions were. According to the mechanics and the general manager, no one from quality control looks at the units until after they are assembled and ready for testing. Following the Safety Board's examination of the facility, and at the request of the UNC Fort Lauderdale facility's general manager/director of engineering and quality, the Safety Board briefed the entire staff of the facility on the above findings. After the briefing, the mechanics and general manager/director of engineering and quality were asked if all of the CSD's and IDG's overhauled as of August 6, 1996, were overhauled in accordance with the manufacturer's overhaul manual, and they all replied that they could not be certain. On August 8, 1996, the FAA's Fort Lauderdale, Florida, FSDO, manager and principal avionics inspector (PAI) for UNC's Fort Lauderdale facility were briefed on the Safety Board's findings. The PMI was not available. Following the briefing, the FSDO office manager stated that his office would take immediate action to correct the problems. On August 9, 1996, the Safety Board was notified by UNC's Fort Lauderdale facility that it had immediately stopped all overhaul work at that facility until corrective action could be completed. On July 30, 1996, Tower Air began, on its own initiative, a fleet-wide campaign to identify all of the CSD's in its inventory that had been overhauled by UNC's Fort Lauderdale facility. Once identified, Tower Air will send the affected CSD's to Sundstrand for examination and overhaul. In addition, Tower Air has asked Sundstrand for a report on any of the above irregularities found during its examination. A review of FAA SDR data from January 1, 1990, through August 27, 1996, was conducted to determine the number of failures of selected Sundstrand CSD models used on jet transport airplanes. The SDR data did not provide information related to the failure mechanism or the overhaul and maintenance history. The SDR data revealed that there were a total of 51 CSD failures, 37 of which resulted in unscheduled landings, and 10 resulted in rejected takeoffs. The reports cited 10 successful CSD disconnects, 9 unsuccessful CSD disconnects, 9 engine shutdowns, 28 CSD low pressure warnings, 20 CSD high temperature indications, 7 fluctuating or low CSD revolutions per minute output, and 12 CSD's that stopped rotating. Sundstrand indicated that the problems found in the CSD's disassembled during this investigation have not been previously reported. However, the large number of SDR reports related to CSD failures, and the lack of information related to those failure mechanisms prompted the FAA to request that Sundstrand examine the CSD's and IDG's during overhaul and document the condition of the fasteners and helicoils and identify the failure mechanism of each unit and provide that data to the FAA. As a result of this investigation the Safety Board issued two Safety Recommendations to the Federal Aviation Administration on December 20, 1996. Recommendation A-96-178, asks the FAA to "require operators of constant speed drives and integrated drive generators overhauled by UNC Accessory Services' Fort Lauderdale facility to remove the units from service, inspect and overhaul them as needed, on a priority basis." Recommendation A-96-179, asks the FAA to "review fastener, helicoil, and failure mechanism data after they are collected by Sundstrand during the overhaul of constant speed drives and integrated drive generators and develop corrective actions if necessary."

Probable Cause and Findings

failure of the constant speed drive (CSD) to disconnect from the generator. Contributing to the cause was the failure of the FAA approved overhaul facility to follow the manufacturer's overhaul manual.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports