Aviation Accident Summaries

Aviation Accident Summary MIA97LA032

SUGARLOAF KEY, FL, USA

Aircraft #1

N9545J

Piper PA-28-180

Analysis

While in cruise flight the engine lost power, and the pilot elected to land on a road. As the airplane touched down the left wing struck the brush on the side of the road, veered left, and turned 180 degrees opposite the direction of travel. Witnesses reported seeing black smoke coming from the engine before impact. The airplane's engine was disassembled, and the examination revealed that the No. 3 connecting rod cap had become detached from the crankshaft assembly, resulting in external damage to the engine. In addition, the remaining connecting rod assemblies were found to be incorrectly installed, and the nuts were all found opposite end down. The No. 2 and No. 4 assemblies were found to be loose.

Factual Information

On December 1, 1996, about 1200 eastern standard time, a Piper PA-28-180, N9545J, registered to a private owner, operating as a Title 14 CFR Part 91, personal flight, crashed during a forced landing near Sugarloaf Key, Florida. Visual meteorological conditions prevailed and no flight plan was filed. The airplane was substantially damage. The private pilot received serious injuries, and one passenger received minor injuries. While in cruise flight the pilot noticed a fluctuation in engine rpm. The engine lost power, and the pilot elected to land on a road. As the airplane touched down the left wing struck the brush on the side of the road, veered left, and turned 180 degrees opposite the direction of travel. Witnesses reported seeing black smoke coming from the engine before impact. The airplane's engine was disassembled under the supervision of the FAA, at Certified Engines Inc., Opa-Locka, Florida, on December 12, 1996. The engine examination revealed that the No. 3 connecting rod cap had become detached from the crankshaft assembly, resulting in external damage to the engine. In addition, the FAA inspector stated, the remaining connecting rod assemblies were found to be "incorrectly installed," and the nuts were "all found opposite end down." The No. 2 and No. 4 assemblies were found to be "loose."

Probable Cause and Findings

a complete loss of engine power due to a disconnected connecting rod cap.

 

Source: NTSB Aviation Accident Database

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