Aviation Accident Summaries

Aviation Accident Summary SEA97FA034

BOISE, ID, USA

Aircraft #1

N75142

Douglas DC-3C

Analysis

The DC-3C took off on runway 10L and immediately executed a right turn followed by a left turn back toward the airport declaring a fire aboard. Dark night visual meteorological conditions existed. Witnesses observed 'flames' or an 'orange glow' coming from the right engine. A small number of aluminum fragments identified from the aft edge of the right engine accessory cowling were found along the ground just short of the ground impact site. These fragments displayed signs of heat distress but no significant melting. An examination of the right engine and accessory section revealed no evidence of a preimpact fire, and sooting and metal splatter on the leading edge of the right horizontal stabilizer was minimal. Spectral analysis of radio transmissions revealed no evidence of significant divergence of engine RPM between the two engines. Postcrash propeller examination revealed approximate blade pitch angles of 18-19 degrees and 30-32 degrees for the right and left propellers respectively upon impact. Propeller slash mark dimensions associated with the right propeller resulted in propeller RPM of approximately 1750 to 2570 over a range of 68 to 100 knots respectively. The first officer advised the PIC (broadcasting over the tower frequency) 'we're gonna stall' approximately 10 seconds before the impact. The aircraft was in a left turn back toward runways 28 left and right when the right wing struck the ground and the aircraft cartwheeled to a stop. A postcrash fire destroyed the cockpit area and inboard right wing.

Factual Information

HISTORY OF FLIGHT On December 9, 1996, at 1803 hours mountain standard time, a Douglas DC-3C, N75142, operated by Desert Air Transport, Inc., doing business as Desert Air, and being crewed by an airline transport rated (ATR) pilot-in-command (PIC) and a commercial pilot serving as first officer (FO), was destroyed during impact with terrain following a loss of control while attempting to return for an emergency landing, at the Boise Air Terminal, Boise, Idaho. Both pilots were fatally injured. Visual meteorological night conditions existed and an instrument flight rules (IFR) flight plan had been filed. The flight, which was a cargo run from Boise, Idaho, to Salt Lake City, Utah, was to have been operated under 14CFR135, and departed Boise at 1800. On December 9, 1997, between 1751:22 and 1752:10, the crew of N75142 contacted Boise (BOI) clearance delivery and requested/received an IFR clearance from Boise to Salt Lake City (refer to ATTACHMENT CT-I), and between 1752:18 and 1752:34, the crew of N75142 contacted BOI ground control and received clearance to taxi from the cargo ramp to runway 10 left (refer to ATTACHMENT CT-II). At 1756:36, the crew contacted the BOI local controller stating that "we're gonna need a uh run-up on the end here," and then radioed at 1759:31, "one four two is ready to go." At 1759:38 the BOI local controller transmitted "runway one zero left cleared for takeoff." The crew of N75142 acknowledged this transmission 4 seconds later. At 1801:56, the BOI local controller inquired "douglas uh one four two you should be on runway heading is that right?" and four seconds later the crew of N75142 radioed "we got a fire on board we're coming back in." At1802:02, the BOI local controller acknowledged the crews' last transmission, inquired as to whether they wished to land on runway 10 right or runway 28, and then provided the current wind. At 1802:14, the crew advised runway 28. Two seconds later the BOI local controller cleared the aircraft to land on any runway and this was acknowledged at 1802:21 with "OK." At 1802:40, the BOI local controller received the following transmission: "we're gonna stall man ah (expletive)" followed nine seconds later by "ahhhhh (expletive)." During these latter transmissions the sound of the aircraft's engine(s) could be heard (refer to ATTACHMENTS CT-III and IV). Three witnesses, two traveling westbound and one eastbound on Gowen Road, and a fourth witness slightly east of the upwind end of runway 10L, observed the aircraft after its takeoff (refer to CHART I). All four witnesses reported seeing "flames" or an "orange glow" coming from the right engine/wing area. The witness located near the runway reported that "it was dark and I could observe the normal blue exhaust coming from the left engine, but observed an orange glow and flames coming from the bottom of the right engine nacelle." The witnesses reported seeing the aircraft turn south and cross over Gowen road and then execute a left turn back toward the runways (10L/R). They also reported the aircraft as low (150-200 feet above ground) during the latter stages of the turn and several expressed concern over whether the aircraft would clear the power lines along the road and the fuel storage tanks just north. Three of the witnesses were consistent in their observation of the aircraft's right wingtip impacting the ground followed by a cartwheel maneuver. One witness reported that "all of a sudden the right wing appeared to dip and the plane appeared to "flip" and land nose first into the ground" (refer to attached witness statements, maps and diagrams). PERSONNEL INFORMATION Pilot-in-Command (PIC) The PIC was 60 years old and possessed an airline transport pilot certificate with a type rating in DC-3 aircraft. His most recent FAA medical examination was conducted August 6, 1996, and he received a Class II certificate with a restriction "Must wear corrective lenses for near and distant vision." According to FAA records, his estimated total civil flight on the date of this examination was reported as 15,150 hours. A pilot log marked "Logbook #4" and bearing the pilot-in-command's name was found at the accident site and subsequently reviewed. The log was opened on June 22, 1990, with a total time of 14,234 hours brought forward, and the last entry within this logbook was dated August 29, 1996, and recorded as a DC-3 flight from Yakutat, Alaska, to Dry Bay, Alaska, and return. The PIC's total flight time, based on this logbook, as of this closing date was 15,288 hours of which 13,819 hours were as pilot-in-command. Company records indicated that the PIC had completed a written airman competency check in accordance with FAR 135.293(a) on September 2, 1996. Additionally, the PIC's logbook showed a 6.7 hour flight from Spokane, Washington, to Long Beach, California, where he served as pilot in command. The aircraft was N2298C, a DC-3, operated by Salair, whom the PIC had been previously employed by. The Salair Chief Pilot confirmed that he gave the PIC an FAR 135.293(b) airman competency/proficiency flight check during that flight. First Officer (FO) The first officer was 57 years old and possessed a commercial pilot license. He also possessed an expired flight instructor certificate as well as a reciprocating flight engineer rating. His most recent FAA medical examination was conducted May 6, 1996, and he received a Class II certificate with a restriction "Must wear lenses for distant - possess glasses for near vision." According to FAA records, his estimated total civil flight on the date of this examination was reported as 8,000 hours. The operator reported the FO's total flight time as 8,862 hours, of which 292 hours were logged in the DC-3, none of which were reported as pilot-in-command time. The operator also reported that the FO was employed solely in a first officer capacity and did not serve as PIC on DC-3 flights with the company. AIRCRAFT INFORMATION N75142, a Douglas DC-3C, serial number 9173, was manufactured in 1944, and at the time of the accident privately owned and leased to the operator. Aircraft logs and records, as well as paperwork found at the crash site, indicated that the aircraft total time at the time of the accident was approximately 34,124 airframe hours. The basic empty weight of the aircraft, according to its last weighing on May 20, 1994, was 17,673 pounds. The maximum gross takeoff weight was reported to be 26,900 pounds. According to information provided by the aircraft manufacturer, the gear ratio between the engine and propellers was 16:9 (1.777). According to Aircraft Flight and Maintenance Log records found at the accident site, N75142 departed Salt Lake City, Utah, at 1125 on Saturday, December 7, 1996, with 600 gallons of aviation gasoline (avgas). Based upon a 2.0 hour flight time for the December 7 flight and a fuel burn of 100 gallons per hour (dual engine operation, block to block) from flight planning information found at the accident site, the aircraft would have arrived at Boise with approximately 400 gallons of fuel. The aircraft did not fly again until the evening of the accident. The aircraft was equipped with a left and right main fuel tank, each with a capacity of 202 gallons, and a left and right auxiliary tank, each with a capacity of 200 gallons. Fueling records maintained by Western Aircraft, Inc. at the Boise airport indicated that N75142 was fueled on December 9, 1996, with a total of 120.0 gallons of 100 low lead octane aviation fuel avgas. The fuel slip indicated that truck number "JT-3" was utilized. An interview of the fueler by the FAA coordinator revealed that this was a written error and that the aircraft had, in fact, been fueled from truck number "FT-3." The total fuel weight at takeoff was estimated at 3,052 pounds. Combining the basic empty weight of 17,673 pounds with an estimated 200 pounds per pilot plus the estimated 3,052 pound fuel load provided a useful load of 5,775 pounds. According to the "Airway Bill/Manifest" from the shipper, 4,109 pounds of cargo consisting of metal stove pipe segments and plastic construction trim material were loaded. The aircraft's gross takeoff weight was estimated to be 25,235 pounds. The aircraft was also equipped with a fire detection and warning system consisting of a thermocouple loop located in each engine accessory area as well as the engine exhaust area. This system, when activated by a fire, would produce an audible "bell" warning in the cockpit as well as a visual (light) indication. The daily log maintained by the Boise airport Air National Guard (ANG) fire department contained an entry indicating that on Saturday afternoon, December 7, 1996, at 1330 local time the "tower reported fire coming from the engine of Desert Air DC-3." An ANG Aircraft Rescue and Firefighting truck at the Boise airport was dispatched to the cargo ramp to investigate the fire, which was reported by a witness to be in the vicinity of the right engine. The aircraft was followed to parking and the log reflected that the "pilot reported it was normal and canceled all those who responded." The captain operating this flight was interviewed and reported that an ANG crash truck drove up to the aircraft but remained only about 10 seconds before departing. He also reported that the first officer (the same first officer on the accident flight) exited the aircraft, inspected the right engine and found nothing unusual and that neither he nor the first officer discussed the matter with the ANG fire truck crew. He speculated that what the ANG crew had observed was torching characteristic of the DC-3 engines. The captain also reported that the flight from Salt Lake City to Boise was uneventful and that the aircraft's fire warning system (bell and light(s)) did not activate during the flight. He also reported that he had never had a backfire while operating this aircraft. METEOROLOGICAL AND ENVIRONMENTAL INFORMATION The 1756 aviation surface weather observation recorded at the Boise airport on the day of the accident reported the following conditions: Winds from 110 degrees magnetic at 10 knots, visibility 10 statute miles, light rain, 6,500 foot overcast conditions, temperature 9 degrees Celsius, dew point 6 degrees Celsius, altimeter 29.49 inches of mercury. The approximate time of sunset at Boise was 1708 local and the sun's elevation was approximately -10 degrees below the horizon at the time of the accident. Dark night environmental conditions existed at the time of the accident. COMMUNICATIONS INFORMATION There was no evidence of any communications difficulties between the aircraft and the respective FAA facilities it was in contact with (refer to ATTACHMENTS CT-I through CT-IV). WRECKAGE AND IMPACT INFORMATION The aircraft crashed at a point one nautical mile short and bearing 105 degrees magnetic from the threshold of runway 28L. The latitude and longitude of the accident site was 43 degrees 33.1 minutes north and 116 degrees 11.7 minutes west respectively (refer to CHART I). The elevation of the site was approximately 2,870 feet above mean sea level (MSL). The first evidence of ground impact was a shallow, narrow smear which quickly broadened to four to six feet in width as it progressed north. Small fragments of green glass were found at the southernmost point of the ground scar (refer to photograph 1). This ground scar progressed north approximately 140 feet and then arced counter-clockwise approximately 110 feet to the final resting place of the forward portion of the aircraft cabin (refer to CHART II). Both propellers and both pilots (in their seats), as well as the upper instrument panel (above the windscreen), were located in the vicinity of the midsection of the ground scar arc (refer to photograph 2 and CHRAT II). The main fuselage came to rest with its longitudinal axis oriented along a 043/223 degree magnetic bearing line (tail northeast). The aircraft displayed extensive post crash fire damage and much of the metal stovepipe which had been part of the cargo load was scattered out the front end of the fuselage. The forward portion of the aircraft fuselage, including the cockpit, had been destroyed by fire and documentation of the cockpit areas was not possible with the exception of those items found clear of the fire area. The left wing exhibited no fire damage and a small amount of diagonal buckling on its upper surface. The right wing exhibited fire damage in the inboard area and extensive upwards bending deformation and shattering from the mid-span area out toward the tip (refer to photographs 3 and 4). Both engines were observed separated from their respective nacelles. The right engine and accessory section was observed in an approximate 45 degree nose down attitude adjacent to the aircraft's left main landing gear and outside the primary post-crash fire area (refer to photographs 5 and 6). The engine's exhaust manifold assembly remained attached to the engine with the exception of 3 sections. These sections were all found along the wreckage distribution path beyond the propellers. The right propeller (all three blades and associated hub assembly) was observed lying on the ground in the southern portion of the arcing ground scar. Two of the three blades showed gradual aftward bending deformation and all three blades were in a relatively flat pitch blade angle (refer to photographs 7 and 8). Several prominent "slash" like cuts were observed in the soil at the point where the ground scar arc commenced (immediately south of the location of the right propeller). The slash marks were both oriented along a 310 degree magnetic bearing line and the perpendicular distance between these two marks was measured to be 28 inches (refer to CHART II). The left engine and accessory section was observed in an approximate 45 degree nose up attitude adjacent to the aircraft's left wingtip and outside the primary post-crash fire area (refer to photographs 9 and 10). The engine's exhaust manifold assembly remained attached to the engine. The left propeller (all three blades and associated hub assembly) was observed lying on the ground in the central portion of the arcing ground scar. Two of the three blades showed extensive bending deformation and all three blades were in a high pitch blade angle (refer to photographs 11 and 12). Both left and right main landing gear were observed in the retracted position. The tail wheel was observed to have been broken free and was under the rear empennage. The right main wheel had sustained extensive post crash fire damage (refer to photograph 13). The left main wheel displayed minimal fire damage (refer to photograph 14). Photograph 15 is a panoramic view of the final resting place of the main airframe and engines. The right wing outboard section from the approximate mid-span point (landing light) to the wingtip displayed extensive upward bending deformation and shattering damage. The vertical and horizontal stabilizers remained attached to the aft empennage. The rudder panel was observed to be attached and the rudder trim tab was in a near neutral position (refer to photograph 16). The left horizontal stabilizer, elevator and trim tab displayed buckling deformation and a small amount of upward bending deformation (refer to photograph 17). The right horizontal stabilizer, elevator and trim tab displayed no major buckling deformation nor any upward or downward bending deformation. The elevator had become partially detached at the outboard hinges (refer to photograph 18). The left horizontal stabilizer was free of particulate material along its de-ice boot. The right horizontal stabilizer, however, displayed several short one inch soot type trails on its upper surface just aft of the de-ice boot and approximately mid span and outboard. Additionally, occasional small silver particles characteristic of melted aluminum were noted adhering to the outboard upper portion of the de-ice boot (refer to photograph 19). Both right and left split flaps were observed in their retracted or "UP" position at the site (refer to photographs 20 and 21). The Janitrol heater, which was installed directly after of the first officer's seat was observed lying on the groun

Probable Cause and Findings

A fire within the right engine compartment of undetermined cause and the pilot-in-command's failure to maintain airspeed above the aircraft's minimum control speed. A factor contributing to the accident was the dark night environmental conditions.

 

Source: NTSB Aviation Accident Database

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