Aviation Accident Summaries

Aviation Accident Summary SEA97LA068

ARLINGTON, WA, USA

Aircraft #1

N36P

Hemingway VARIEZE

Analysis

The pilot, who reported approximately 132 hours of flight experience of which one and three-quarters hour were in this make/model aircraft, intended to conduct high speed taxi tests of the aircraft, and then transition directly to a flight test. During the first taxi test run down the runway the pilot rotated and 'the aircraft lifted off rapidly and steeply.' The pilot reported that he was able to successfully re-land but felt that he had 'over-controlled' the aircraft.' After returning to the threshold of runway 34 he initiated a second taxi run down the runway and reported that 'just before I planned to shut down the engine it (the aircraft) lifted off just as abruptly as the first time at a very steep attitude, also higher than before, about 20 feet.' During the attempted recovery the aircraft struck the runway nose down and left wing low and slid to a stop. An observer to the accident located near an adjacent taxiway reported a wind gust coincident with the time of the second nose rotation. Winds at the Arlington airport were reported as 300 degrees magnetic at 10 knots at 1253 hours.

Factual Information

On February 24, 1997, approximately 1245 Pacific standard time, a homebuilt Hemingway Varieze, N36P, registered to and being operated by the builder, a private pilot, was substantially damaged during a loss of control while executing a high speed taxi run on runway 34 at the Arlington airport, Arlington, Washington. The pilot sustained minor injuries. Visual meteorological conditions existed and no flight plan had been filed. The flight, which was a test taxi/flight, was to have been operated under 14CFR91, and was to have been local. The pilot reported to an FAA inspector that he intended to conduct high speed taxi tests of the aircraft, and then transition directly to a flight test. During the first taxi test run down the runway the pilot rotated and "the aircraft lifted off rapidly and steeply." The pilot reported that he was able to successfully re-land and felt that he had "over-controlled" the aircraft. The pilot returned to the threshold of runway 34 and initiated a second taxi run down the runway. He reported that "just before I planned to shut down the engine it (the aircraft) lifted off just as abruptly as the first time at a very steep attitude, also higher than before, about 20 feet." The aircraft struck the runway nose down and left wing low and slid to a stop. The pilot reported approximately 132 hours of flight experience of which one and three-quarters hour were in this make/model aircraft. An observer to the accident located near an adjacent taxiway reported a wind gust coincident with the time of the second nose rotation. Winds at the Arlington airport were reported as 300 degrees magnetic at 10 knots at 1253 hours.

Probable Cause and Findings

The pilot's failure to maintain control of the aircraft. Factors contributing to the accident were the pilot's lack of total experience in the type of aircraft and the gusty wind conditions.

 

Source: NTSB Aviation Accident Database

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