Aviation Accident Summaries

Aviation Accident Summary ANC97LA046

NOME, AK, USA

Aircraft #1

N555CG

Beech G18S

Analysis

Shortly after reaching cruise altitude, the pilot heard a loud noise and felt a vibration in the left engine. He shut the left engine down, and returned to his departure airport. Upon landing, it was discovered that approximately eight inches of a propeller blade tip attached to the left engine had separated and impacted the nose section of the airplane. The blade tip damaged a former in the nose, and then traveled into the right engine nacelle. A small nick was observed on the remaining blade surface that coincided with the fracture plane.

Factual Information

On March 21, 1997, about 1715 Alaska standard time, a wheel equipped Beech G-18S airplane, N555CG, sustained substantial damage when approximately eight inches of a propeller tip separated from a propeller blade on the left engine and penetrated the nose of the airplane, coming to rest in the right engine nacelle. The solo airline transport certificated pilot was not injured. The 14 CFR Part 135 cargo flight departed Nome, Alaska, about 1715, and was en route to Gamble, Alaska. According to the operator's chief pilot, the pilot of the accident airplane reported the propeller tip separation occurred shortly after reaching cruise altitude. The pilot shut down the left engine, returned to Nome and landed without incident. An examination of the remaining portion of the propeller blade disclosed a small nick on the surface of the blade that coincided with the juncture of the fracture plane. The accident airplane received damage to a former in the nose section, just in front of the radio bay.

Probable Cause and Findings

fracture of a propeller blade tip.

 

Source: NTSB Aviation Accident Database

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