Aviation Accident Summaries

Aviation Accident Summary ATL97LA140

GREENVILLE, SC, USA

Aircraft #1

N738SZ

Cessna 172N

Analysis

The pilot stated that, the initial takeoff started from the (approach) end of runway 36, and that he had applied full power. At about the midfield point, the airplane lifted off. However, the pilot did not feel there was sufficient power to take off, so he aborted the takeoff. He said he pulled the power all the way back, and the airplane descended nose first, collided the runway nose gear first, and nosed over. A witness stated that during the takeoff roll, the airplane began to porpoise before the nose gear collided with the runway. Examination of the airplane failed to disclose a mechanical problem. The pilot did not report experiencing a mechanical problem with the airplane during the attempted takeoff. According to the pilot operation handbook, normal takeoff ground run should have been about 478 feet. The runway was 5393 feet in length.

Factual Information

On September 25, 1997, about 1915 eastern daylight time, a Cessna 172N, N738SZ, collided the nose gear with the runway and nosed over at Greenville Downtown Airport in Greenville, South Carolina. The personal flight operated under the provisions of Title 14 CFR Part 91 and visual flight rules. No flight plan was filed for the touch and go practice flight. Visual meteorological conditions prevailed. The private pilot was not injured, and the airplane was substantially damaged. The flight originated from Greenville, South Carolina, at 1914. The pilot stated that, the initial takeoff started from the end of the runway and he had applied full power. At the mid field point of runway 36, the airplane lifted off. However, the pilot did not feel that the airplane had sufficient power to takeoff, so he aborted the takeoff. The pilot said he pulled the power all the way back and the airplane descended nose first on the runway. The nose gear collapsed, and the airplane nosed over. An eyewitness stated that during the takeoff roll, the airplane began to porpoise before the nose gear collided with the runway. An examination of the airplane failed to disclose a mechanical problem, and the pilot did not report experiencing a mechanical problem with the airplane during the attempted takeoff. The pilot's operation handbook states that the normal takeoff ground run is 478 feet. Runway 36 is 5393 feet long.

Probable Cause and Findings

the pilot's improper use of the elevator control and delayed liftoff during takeoff, which resulted in an inadvertent porpoise, collision with the runway, and collapse of the nose gear as he aborted the takeoff.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports