Aviation Accident Summaries

Aviation Accident Summary SEA98LA050

SEATTLE, WA, USA

Aircraft #1

N5245P

Hughes 369E

Analysis

The pilot stated that he was making a normal approach until about 30 feet in the air on short final, when he experienced a loss of power. After the resulting hard landing, the engine was still running and shut down by the pilot. Pressure and vacuum checks were performed on the engine fuel system and the engine was run successfully. Upon reassembly of the helicopter, the airframe mounted anti-ice fuel filter element was found to be restricted and the bypass switch was inoperative.

Factual Information

On March 21, 1998, approximately 1745 Pacific standard time, a Hughes 369E, N5245P, registered to and operated by Trident Seafoods Corporation, was substantially damaged during a hard landing at Boeing Field, Seattle, WA. The pilot and one passenger received minor injuries. The two remaining passengers received no injuries. Visual meteorological conditions prevailed and no flight plan had been filed. The flight, which was for personal purposes, was operated under 14CFR91, and originated from Barnes Island, WA approximately 40 minutes prior to the accident. During an interview, the pilot stated that everything was normal until he was about 30 feet in the air on short final. At that point he experienced a loss of power but the engine did not quit. After the resulting hard landing, the engine was still running and shut down by the pilot. The helicopter was examined on March 23, 1998 after it had been moved to a hanger. Pressure and vacuum checks were performed on the engine fuel system. Fuel screens were also examined. No discrepancies were noted. The engine was later transported by the insurance company to ACRO Aerospace in Vancouver, BC, Canada. The Allison representative who observed the testing there reported that the engine started and ran normally during the tests except for a discrepancy about 40 minutes into the test when the engine failed to accelerate from idle. The scroll to PC filter tube B-nuts were found to be loose and the engine again performed normally after tightening. This line had previously been removed as part of the system pressure tests.

Probable Cause and Findings

Loss of engine power due to a restricted fuel system filter.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports