Aviation Accident Summaries

Aviation Accident Summary CHI93IA078

DETROIT, MI, USA

Aircraft #1

N452US

FOKKER F-28 MK 1000

Analysis

THE CAPTAIN OBTAINED NO RESPONSE TO NOSE-UP STABILIZER TRIM DURING DESCENT. NORMAL NOSE-DOWN TRIM REMAINED OPERABLE; ALTERNATE TRIM WAS NOT ATTEMPTED. THE CREW REPORTED A JAMMED STABILIZER AND LANDED WITH NOSE-DOWN TRIM. DISASSEMBLY OF THE HORIZONTAL STABILIZER CONTROL UNIT SHOWED INADEQUATE LUBRICANT AND EXTENSIVE CORROSION IN A GEARBOX. THE AIRFRAME MANUFACTURER'S PROCEDURE FOR REPLENISHING THE GEARBOX LUBRICANT COULD RESULT IN UNDERSERVICING. THE OPERATOR OBSERVED A GEARBOX SERVICE INTERVAL WHICH WAS 250% OF THE MANUFACTURER'S RECOMMENDATION.

Probable Cause and Findings

IMPROPER LUBRICATION OF THE HORIZONTAL STABILIZER GEARBOX BY COMPANY MAINTENANCE PERSONNEL. A FACTOR WAS THE MANUFACTURER'S INADEQUATE SERVICE PROCEDURE.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports