Aviation Accident Summaries

Aviation Accident Summary ATL93FA062

TULLAHOMA, TN, USA

Aircraft #1

N405PC

CESSNA 402B

Analysis

A WITNESS REPORTED THAT THE AIRPLANE USED THE ENTIRE RUNWAY TO GET AIRBORNE, REACHED ABOUT 300 FT AGL AFTER LIFTOFF, AND DRIFTED RIGHT. IT THEN IMPACTED TREES ABOUT 1/3 MI FROM THE DEPARTURE END OF THE RUNWAY. DAMAGE TO THE TREES INDICATED THAT THE AIRPLANE WAS IN A RIGHT BANK AT IMPACT. BOTH PROPELLERS SHOWED EVIDENCE OF ROTATION AT IMPACT. ESTIMATED WEIGHT CALCULATIONS SHOWED THAT THE AIRPLANE WAS AT LEAST 165 LBS IN EXCESS OF MAX GROSS WEIGHT; THIS DOES NOT INCLUDE AN UNKNOWN AMOUNT OF FUEL ON BOARD PRIOR TO THE LAST REFUELING.

Factual Information

HISTORY OF FLIGHT On March 23, 1993, at about 0328 central standard time, a Cessna 402B, N405PC, collided with trees and terrain shortly after takeoff from the Tullahoma Regional Airport in Tullahoma, Tennessee. The airline transport pilot was fatally injured. The aircraft was operated under 14 CFR Part 135 by Springdale Air Service of Springdale, Arkansas. The aircraft was destroyed. Night, visual meteorological conditions prevailed at the time, and an instrument flight rules flight plan was filed for the non- scheduled cargo flight to Harrisburg, Pennsylvania. The flight was originating at the time of the accident. The purpose of the flight was to transport photographic prints and film which had been processed at the Walmart processing facility in Tullahoma. Reportedly, the accident pilot arrived in Tullahoma from Harrisburg earlier in the evening in N405PC. The pilot refueled the aircraft, and loaded the cargo, which consisted mainly of vinyl bags of processed photographs. An employee at Walmart reported that the weight of the delivered cargo was 1,198.5 pounds. One of the Walmart employees reported that the pilot did not mention any aircraft abnormalities or problems during casual conversation. At 0311, a man who identified himself as the pilot of SPG100 (a company call sign for N405PC) requested an instrument flight rules (IFR) clearance from Tullahoma to Harrisburg, and advised that the departure runway would be runway 36. At 0313, the Nashville, Tennessee Automated Flight Service Station (AFSS) issued an IFR clearance to SPG100. No inflight communications were reported from SPG100 prior to the accident. A student who was studying in his trailer at the south end of the airport reported that he heard an aircraft "testing its' engines", prior to the time of the accident. He reported that he heard the aircraft go to full throttle about three times, about 3 to 4 minutes apart. He was familiar with the operations of this aircraft, and stated that the engine sound "didn't quite sound right." He stated that the aircraft took off about 10 or 15 minutes after 3 a.m. Another witness was camping on the east end of the airport. He stated that the aircraft used the entire runway to get airborne, then drifted right. After the aircraft passed a building materials store, it lost altitude. He estimated that the aircraft was less than 300 feet above ground level. He saw no flash prior to the accident. He stated that "it sounded as if he had trouble gaining full power for takeoff." A police patrolman reported that at about 0328, he saw an orange object, or "glow", in the air, in the direction of the airport. The glow began to grow dim, and he observed a large, mushroom shaped "fireball" above the treeline. About two minutes later, he arrived on the scene of the accident. He stated that several small explosions occurred after his arrival upon the crash scene. PERSONNEL INFORMATION Information on the pilot is included in this report. See "First Pilot Information." AIRCRAFT INFORMATION Information on the aircraft is included in this report. See "Aircraft Information." METEOROLOGICAL INFORMATION Night, visual meteorological conditions existed at the time of the accident. Several witnesses reported that at the approximate time of the accident, heavy rain was present. Meteorological information is included in this report under "Weather Information." WRECKAGE AND IMPACT INFORMATION The aircraft crashed in the front yard of a single family dwelling, about one third mile northeast of the departure end of runway 36 (Tullahoma Airport). The wreckage path was about 300 feet in length, and the magnetic heading from the first observed impact marks to the main wreckage was about 056 degrees. The main wreckage was found inverted, on a two lane, paved asphalt road. A wreckage distribution diagram is included as an attachment to this report. On each side of the road where the main wreckage was found were storm drainage ditches, filled with water. The right, nose baggage door and the right engine top cowling were found in the ditch, partially submerged in the water. Soot, along with heat and fire damage, was observed above the level of the water. Below the level of the water, no heat or fire damage or soot was observed. The right engine propeller was found separated from the engine, about 36 feet southwest of the main wreckage. The left propeller remained attached to the engine. The landing gear were found in the retracted position. The left and right wing flaps were found extended about 15 degrees. All aircraft fuel tanks were destroyed; no residual fuel was found. Both the left and right fuel selector valves were found in the "left main" tank position. MEDICAL AND PATHOLOGICAL INFORMATION A post mortem examination of the pilot was performed by Dr. Julia C. Goodin, M.D., Office of the Medical Examiners, Nashville, Tennessee. She reported that the cause of death was from multiple injuries and thermal injury, including rib fractures, perforating injuries to the right chest with lacerations of the lungs, liver, heart, and diaphragm. Toxicological testing for carbon monoxide, alcohol, basic, acidic, and neutral drugs was negative. TESTS AND RESEARCH The right engine was disassembled and examined at the manufacturer's facility in Mobile, Alabama following the accident. The left engine fuel manifold valve, left engine driven fuel pump, and left engine throttle control were also inspected at this examination. The results are included as an attachment to this report (re: Teledyne Continental Motors Analytical Inspection Report). The left engine was inspected at a wreckage storage facility in Jefferson, Georgia. The engine oil sump area had impact damage; the camshaft gear was bent and the engine could not be turned by hand. The engine cylinders were removed, and there was no evidence of internal malfunction or failure observed. The propellers were disassembled and inspected at the manufacturer's facility in Vandalia, Ohio. An inspection report is included as an attachment to this report (re: Propeller Teardown Inspection Report provided by McCauley Accessory Division). The turbochargers were disassembled and inspected in conjunction with the right engine inspection in Mobile, Alabama. The disassembled parts were subsequently inspected with a manufacturer's representative at a storage facility in Jefferson, Georgia. An inspection report is included as an attachment to this report (re: Garrett Turbocharger Inspection Report). The aircraft weight at the time of takeoff was estimated using the following information: Aircraft Empty Weight: 4221 lbs. Engine Oil: 49 " Aircraft Fuel Added to N405PC Prior to Flight: 779 " Pilot: 218 " Cargo: 1198 " Total: 6465 " Maximum Takeoff Weight: 6300 lbs. The aircraft empty weight was obtained from information provided by the operator. The cargo weight was obtained from Walmart personnel. Due to fire and water damage, the cargo could not be accurately weighed after the accident. The distribution of the cargo was not reconstructed due to impact and fire damage. The amount of fuel in the tanks prior to the last fueling was not known; that amount is not included in the total weight above. ADDITIONAL INFORMATION The aircraft wreckage was released to: Keith Wright AIG Aviation, Inc. Atlanta, Georgia.

Probable Cause and Findings

THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE DURING TAKEOFF. FACTORS WHICH CONTRIBUTED TO THE ACCIDENT WERE: THE PILOT'S FAILURE TO ENSURE THAT THE AIRPLANE MAXIMUM GROSS TAKEOFF WEIGHT WAS NOT EXCEEDED, THE DARK NIGHT, AND RAIN.

 

Source: NTSB Aviation Accident Database

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