Aviation Accident Summaries

Aviation Accident Summary SEA93LA072

RIVERTON, WY, USA

Aircraft #1

N821SC

PIPER PA-32-260

Analysis

THE PILOT OBSERVED THAT THE AIRCRAFT WAS NOT PRODUCING EXPECTED POWER, AND ASSURED DURING THE TAKEOFF GROUND RUN THAT THE PROPELLER, THROTTLE, AND MIXTURE CONTROLS WERE FULL FORWARD. THE TAKEOFF USED ABOUT HALF THE LENGTH OF THE 8202 FOOT RUNWAY. THE AIRCRAFT LIFTED OFF, CLIMBED TO ABOUT 50 FEET AND WOULD NOT CLIMB. THE AIRCRAFT STRUCK A LIGHT POLE AND CRASHED IN A FIELD ABOUT 1.5 MILES FROM THE AIRPORT. ALTHOUGH THE PILOT NOTED THAT HE HAD EXPECTED TO TAKEOFF GROUND RUN TO BE ABOUT 2000 FEET, HE FAILED TO ABORT THE TAKEOFF.

Probable Cause and Findings

THE PILOT DID NOT PERFORM AN ABORT OF THE TAKEOFF AFTER OBSERVING A PARTIAL LOSS OF POWER. FACTORS INCLUDE IMPROPER USE OF THE MIXTURE CONTROL.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports