Aviation Accident Summaries

Aviation Accident Summary ATL91FA039

ARDEN, NC, USA

Aircraft #1

N4589V

BEECH 35

Analysis

DURING THE INITIAL CLIMB AFTER TAKEOFF, THE ENG LOST POWER. SUBSEQUENTLY, THE ACFT COLLIDED WITH TREES AND CRASHED. WATER WAS FOUND IN A FUEL LINE (BTN THE FUEL SELECTOR VLV AND ELECTRIC FUEL PUMP), ELECTRIC BOOST PUMP MANIFOLD, AND CARBURETOR (CARB) INLET STRAINER; HOWEVER, THE FUEL SYSTEM WAS DAMAGED DURING IMPACT AND FIRE SUPPRESSANT CHEMICALS WERE SPRAYED ON THE WRECKAGE. A CHECK OF THE CARB SHOWED THAT IT WAS PROVIDING A LEAN MIXTURE AT LOW POWER SETTINGS AND A RICH MIXTURE AT HI POWER SETTINGS. A TEARDOWN OF THE CARB REVEALED A CRYSTALLINE SUBSTANCE ON THE CARB DIAPHRAGM, AN IMPROPER METERING JET, AND THAT 5 SHIMS WERE INSTALLED IN THE CARB REGULATOR DIAPHRAGM SPRING MECHANISM. THE BENDIX OVERHAUL MANUAL ALLOWED A MAXIMUM OF 2 SHIMS. DURING A POST-ACDNT CHECK, THE ENG OPERATED NORMALLY WITH THE ELECTRIC FUEL PUMP ON, BUT THE ENG STOPPED RUNNING WHEN THE ELECTRIC PUMP WAS TURNED OFF.

Probable Cause and Findings

FOR UNDETERMINED REASONS, THE ENGINE LOST POWER.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports