FORT LAUDERDALE, FL, USA
N6640R
BEECH C-45H
TWO PAX STATED THAT THE FLT ENCOUNTERED TURBULENCE DURING THE APCH. THE ACFT LANDED HARD & THE LT MAIN LANDING GEAR COLLAPSED. THE ACFT THEN YAWED TO THE LT & THE NOSE & RT MAIN LANDING GEARS COLLAPSED DUE TO THE SIDELOAD. EXAM OF THE LT MAIN LANDING GEAR ASSY REVEALED THAT THE WALKING BEAM FAILED DUE TO OVERSTRESS WHICH ALLOWED THE GEAR TO COLLAPSE. EXAM OF THE ACFT REVEALED THAT THE RT ENG SEPARATED IN A DOWNWARD DIRECTION. THE LT ENG WAS PARTIALLY ATTACHED BUT DEFLECTED IN A DOWNWARD DIRECTION.
HARD LANDING DUE TO FAILURE OF THE PILOT-IN-COMMAND TO MAINTAIN THE PROPER DESCENT RATE. CONTRIBUTING TO THE ACCIDENT WAS THE TURBULENCE ENCOUNTERED DURING THE APCH.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports