Aviation Accident Summaries

Aviation Accident Summary CHI00LA069

OLATHE, KS, USA

Aircraft #1

N711VS

Beech A36

Analysis

The aircraft impacted terrain approximately 900 feet from the end of the runway during a simulated engine failure. The pilot had just finished a flight review when he requested to simulate an engine failure in the pattern with the instructor. The pilot said, 'I pulled the power back to idle after we passed the end of runway 18. As I was turning to runway 18 I...lowered the landing gear...When we both came to the conclusion that we were not going to be able to make the runway without power, I advanced the throttle. The engine coughed a couple of times and never developed power.' A Federal Aviation Administration inspector interviewed the instructor. When asked if he saw the pilot pull the propeller control full aft, he responded, 'Yes.' When asked if he saw the pilot return it to full forward at any time, he responded 'No.' The pilot maneuvered the aircraft away from a road and runway approach lights ultimately coming to rest in a plowed farm field. A post accident functional test of the engine showed that the engine produced power at idle and low power settings.

Factual Information

On February 12, 2000, at 1323 central standard time, a Beech A36, N711VS, piloted by a commercial pilot, sustained substantial damage during a forced landing near Olathe, Kansas. The 14 CFR Part 91 instructional flight was operating in visual meteorological conditions. The pilot had filed an instrument flight rules flight plan that was subsequently cancelled. The pilot and the certified flight instructor reported no injuries. The local flight originated from the Johnson County Executive airport, Olathe, Kansas. The pilot reported that the flight originated at 1310. The pilot, in a written statement, stated that he had just completed the BFR when he requested to practice a simulated engine failure with the instructor. The pilot said, "I pulled the power back to idle after we passed the end of runway 18. As I was turning to runway 18, I slowed the aircraft to approximately 80 knots. [The instructor] mentioned that he thought the plane would descend too rapidly from where we started to make it. I thought we had a good chance based on my experience with the plane and went ahead and lowered the landing gear, thinking that I would want it down even if I needed to apply power to make the runway. The wind was reported at about 6 knots. When we both came to the conclusion that we were not going to be able to make the runway without power, I advanced the throttle. The engine coughed a couple of times and never developed power." The aircraft came to rest in a plowed farm field. During a post accident examination, performed by the Federal Aviation Administration, the throttle was found full forward, the mixture was found full forward, and the propeller control was found full aft. During an interview with a FAA inspector, the instructor was asked about the position of the powerplant controls. When asked if he touched or moved any of the controls, he replied "No." When asked if he saw the pilot pull the propeller control aft, he responded "Yes." When asked if he saw the pilot return it to full forward any time after that, he replied "No." According to FAA Advisory Circular 61-23C, "Pilot's Handbook of Aeronautical Knowledge", "When power settings are being decreased, reduce manifold pressure before RPM. When power settings are being increased, reverse the order - increase RPM first, then manifold pressure." According to FAA Inspector statements, post flight examinations of the aircraft revealed, "both fuel tanks were indicating about 3/4 full. All three propeller blades were bent." After the accident a functional engine test was performed. According to the FAA inspector who witnessed the test "the engine was started and run for a short period of time; long enough to perform a magneto check at idle and 1400 RPM. The magneto check was normal in both instances. The engine idled at 700 RPM with the throttle pulled all the way out to the idle position. There was no indication of excessively lean or rich mixture at idle that would contribute to the engine not idling properly."

Probable Cause and Findings

the pilots improper use of powerplant controls. A factor in the accident was the plowed farm field.

 

Source: NTSB Aviation Accident Database

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