Aviation Accident Summaries

Aviation Accident Summary IAD00LA042

GETTYSBURG, PA, USA

Aircraft #1

N91480

Maule M-4-220C

Analysis

The pilot was performing an engine run-up when the engine backfired. Shortly after the engine backfired white smoke was visible coming from the underside of the engine cowling. The pilot turned off the fuel selector switch and exited the airplane, where he noted the underside of the engine engulfed in flames. Examination of the airplane revealed that the fuel drain located under the engine was found in the open position.

Factual Information

On May 15, 2000, at 1530 Eastern Daylight Time, a Maule M-4-220C, N91480, was substantially damaged by fire that started in the engine compartment during engine run-up at a private airstrip in Gettysburg, Pennsylvania. The certificated commercial pilot/owner was not injured. Visual meteorological conditions prevailed for the personal flight conducted under 14 CFR Part 91. No flight plan was filed. According to the pilot/owner's written statement, he said: "At 1530 hours on Sunday...I pre-flighted the aircraft, draining the sumps for water, removing the gust locks, and checking the cowl openings for bird nests. The plane had been there for two weeks with wings level and the fuel selector on "off". There were a few drops of gook in the right tank. I started the engine with the fuel select on the left tank and taxied to the top of the incline to face a westerly breeze for the run-up. With the right wing uphill, I switched to the right tank and checked the [magnetos] at 2000 rpm, noting the normal drop off (250-260), then cycled the prop governor with a sluggish drop since everything was not warmed up. When I applied carburetor heat, the rpms dropped rapidly in the 300 range, so I pushed the control forward thinking the anomaly might clear if I had sufficient water in the system to have already formed an ice blockage in the venturi. I gradually applied [carburetor] heat and the control seemed to come back further than usual and more easily than normal at the extremity of range, but a similar larger and more rapid drop accompanied by backfiring had caused me to push the control forward to keep the prop turning. I raised the rpm to about 2000 to solve the problem with a third try on the carburetor heat and this time the engine stopped followed by white smoke on both sides of the cowling, so I opened my door and turned the fuel selector off, and looked outside to see the entire underside of the engine in flames. I turned off the ignition and stepped outside." The pilot also stated that when he saw the flames coming from underneath the airplane, he reached back in the airplane and turned off the ignition. He did not reach for the fire extinguisher that was in front of him. The pilot made four trips over three hundred yards in his truck to get water before the fire company arrived and prevented destruction of the wheels, tail, and outer wing sections. A Federal Aviation Administration (FAA) inspector performed an on-site examination on May 15, 2000. According to the inspector's written statement, he said: "The aircraft sustained substantial damage when it caught on fire on its pre-take-off run-up...the fuel strainer bowl drain mounted on the forward left hand side of the firewall was found in the open position. I spoke with the local fire chief who responded to the fire and he stated without question that neither he or the firemen had opened the valve. "The exhaust system on the left side of the engine is located forward of the suspect drain valve. The visual appearance of the engine compartment would indicate that the area of most heat damage was on the left hand side. If there were other maintenance items that caused the back fire, that evidence was destroyed by fire." In the pilot's written statement, he responded to the inspector's finding: "I distinctly recall pressing down on the drain valve to make sure it was seated [during] the preflight [inspection], because I have seen it dripping without this special attention. I do not remember opening it following the incident, but I did open both the underside drains at the low point of the system." The pilot held a commercial certificate for single and multi-engine land airplanes, with an instrument rating. He reported a total of 4,398 flight hours with 104 flight hours in make in model.

Probable Cause and Findings

The pilot's improper pre-flight which resulted in the fuel strainer valve being left in the open position.

 

Source: NTSB Aviation Accident Database

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