Aviation Accident Summaries

Aviation Accident Summary DEN90IA189

DENVER, CO, USA

Aircraft #1

N9044U

BOEING 737-222

Analysis

SHORTLY AFTER PUSHBACK IT WAS NOTICED THAT THE #2 ENG DOOR 2 RIGHT HANDLE WAS NOT FLUSH. THE ENG WAS SHUT DOWN AND GROUND MAINT PERSONNEL CLOSED THE DOOR FROM THE OUTSIDE. THE CABIN THEN BEGAN TO FILL WITH DENSE SMOKE. THE CAPTAIN, USING RADIO AND AN OPEN WINDOW, WAS UNSUCCESSFUL IN GETTING A JETWAY TO THE AIRPLANE, AND THE CREW AND PAX EXITED USING SLIDES. IT WAS LATER DETERMINED THAT THE BATTERY BUSS RELAY (R1) AND BATTERY TRANSFER RELAY (R2) HAD FAILED. THE AIRPLANE HAD BEEN PUSHED BACK AT GATE B-8, AND HAD RECEIVED CLEARANCE TO GATE B-20 FOR THE EVACUATION. THERE WAS NO JETWAY OPERATOR PRESENT, AND GROUND PERSONNEL ARE NOT CROSS-TRAINED TO OPERATE A JETWAY. WHEN THE #2 ENG WAS SHUT DOWN, THE ELECTRICAL TRANSFER SYSTEM PICKED UP THE LOAD. THE FLIGHTCREW DID NOT POWER THE RIGHT BUS FROM THE APU.

Probable Cause and Findings

THE FAILURE OF THE FLIGHT CREW TO FOLLOW EMERGENCY PROCEDURES/DIRECTIVES. FACTORS WERE THE FAILURE OF THE AIRCRAFT ELECTRICAL SYSTEM (RELAYS) AND THE FAILURE OF THE COMPANY TO PROVIDE A JETWAY OPERATOR.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports