Aviation Accident Summaries

Aviation Accident Summary ANC89FA069

GIRDWOOD, AK, USA

Aircraft #1

N524EH

BELL 412

Analysis

WHILE IFR AT 10,000 FEET OVER MOUNTAINOUS TERRAIN, THE HELCIOPTER EXPERIENCED VIOLENT VERTICAL VIBRATIONS, WHICH CONTINUED UNTIL THE CRASH-LANDING ABOUT FIVE MINUTES LATER. ON BOARD WEATHER RADAR WAS USED TO GUIDE THE HELICOPTER AROUND THE MOUNTAIN TOPS, WHICH WERE IN THE CLOUDS. AT ABOUT 200 FEET ABOVE THE GROUND, THE HELICOPTER CAUGHT FIRE, TAIL ROTOR CONTROL WAS LOST, BOTH ENGINES QUIT, AND CYCLIC CONTROL BECAME UNRESPONSIVE. THE HELICOPTER WAS DESTROYED BY POST-CRASH FIRE. ABOUT ONE HOUR OF FLT TIME EARLIER, THE HELICOPTER HAD UNDERGONE AN INSPECTION, DURING WHICH THE MAIN ROTOR FLIGHT CONTROL SYSTEM BOLTS HAD BEEN RETORQUED. ALL BUT ONE OF THESE BOLTS WERE FOUND IN THE WRECKAGE. HOWEVER, THE ROD END FOR THE MISSING BOLT WAS FOUND.

Probable Cause and Findings

A MAIN ROTOR FLIGHT CONTROL BOLT (PART NUMBER 20-057-6-38D) CAME OUT OF ITS ROD END BEARING WHILE IN FLIGHT DUE TO THE BOLT BEING IMPROPERLY TORQUED DURING MAINTENANCE.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports