Aviation Accident Summaries

Aviation Accident Summary DEN89FA155

MINOT, ND, USA

Aircraft #1

N5295H

PIPER PA-16

Analysis

AS THE PLT TURNED ON FINAL APCH TO LND, HE HEARD A 'THUD,' THEN THE ACFT ENTERED AN UNCONTROLLED LEFT TURN. AFTER TURNING ABOUT 360 DEG, IT IMPACTED THE GROUND IN A LEFT WING LOW, NOSE LOW ATTITUDE. AN INVESTIGATION REVEALED A FAILUREOF THE AIRFRAME TUBING AT THE LOWER FORWARD DOOR FRAME. THE FAILURE WAS IN THE AREA OF A CONGLOMERATE WELD WHERE THE TUBING WAS PART OF THE DOOR FRAME, FIRE WALL/ENGINE MOUNT, & RIGHT FORWARD LIFT STRUT SUPPORT. AN EXAM REVEALED THE TUBING HAD SEPARATED PRIOR TO IMPACT. APRX 3/4 OF THE FRACTURE WAS THE RESULT OF CORROSION; THE REMAINING FRACTURE WAS FROM OVERLOAD, BUT NOT DUE TO IMPACT. WITH THIS FAILURE, THE LEADING EDGE OF THE RIGHT WING WOULD TWIST UPWARD & THE ENGINE (WITH POWER) WOULD MOVE UP & TO THE LEFT. PIPER SERVICE BULLETING #819, SUBJECT: FUSELAGE DOOR FRAME TUBE CORROSION, DATED 2/28/86, ADDRESSED THE HAZARD OF CORROSION IN THIS AREA.

Probable Cause and Findings

FAILURE OF THE AIRFRAME TUBING (LONGERON) AT THE LOWER FORWARD DOOR FRAME DUE TO CORROSION. A CONTRIBUTING FACTOR WAS FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH SERVICE BULLETIN #819.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports