Aviation Accident Summaries

Aviation Accident Summary LAX89LA269

CHANDLER, AZ, USA

Aircraft #1

N514A

BELLANCA 14-19

Analysis

THE PLT RPTD THAT THE FUEL PRESSURE INCREASED TO 10 PSI FOLLOWED BY A LOSS OF POWER. THE PILOT LEANED THE MIXTURE CONTROL BUT TO NO AVAIL. THE AIRPLANE CRASHED ADJACENT TO THE AIRPORT. THE PLT RPTD THAT A MECHANIC ADJUSTED THE FUEL PRESSURE BEFORE DEPARTING ON THE ACCIDENT FLT; THE MECHANIC DENIED THAT HE ADJUSTED THE FUEL PRESSURE AND ACCUSED THE PLT OF PERFORMING THE ADJUSTMENT. THE FUEL PUMP OPERATED NORMALLY WHEN FUNCTIONALLY TESTED. THE CARBURETOR WAS BROKEN AND COULD NOT BE TESTED. BOTH FUEL TANKS CONTAINED ADEQUATE FUEL.

Probable Cause and Findings

AN ENGINE POWER LOSS FOR UNDETERMINED REASONS.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports