Aviation Accident Summaries

Aviation Accident Summary LAX87LA294

TAFT, CA, USA

Aircraft #1

N917B

BELL 47D-1

Analysis

THE PLT RPRTD THE ENG LOST POWER AT ABOUT 300' AGL AFTER THE HELICOPTER HAD FLOWN APRX 2.7 HRS WITHOUT REFUELING. HE INITIATED AN AUTOROTATIVE LANDING; HOWEVER, BEFORE TOUCHDOWN, THE MAIN ROTOR BLADES CONTACTED & SEVERED THE TAIL BOOM. AN EXAM REVEALED THE FUEL TANK WAS EMPTY. NO SIGNS OF FUEL LEAKAGE WERE FOUND. THE HELICOPTER HAD BEEN EQUIPPED WITH A 210 HP FRANKLIN ENG IAW A SUPPLEMENTAL TYPE CERTIFICATE. THERE WAS NO FACTORY DATA ON FUEL CONSUMPTION RATES FOR THIS CONFIGURATION. OTHER OPERATORS, WHO OPERATED THIS MAKE & MODEL OF HELICOPTER, ESTIMATED THE FUEL CONSUMPTION WAS APRX 12 GAL/HR. AFTER THE ACDNT, THE PLT RPRTD HE MEASURED THE FUEL CAPACITY OF THE HELICOPTER FUEL CELL. HE STATED THE CELL WOULD HOLD ONLY 26.5 GAL OF FUEL, INSTEAD OF '29' AS INDCD BY A STICK-ON MARKER THAT HAD BEEN INSTALLED ON A PREVIOUSLY PAINTED PLACARD.

 

Source: NTSB Aviation Accident Database

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