Aviation Accident Summaries

Aviation Accident Summary DEN84LA299

MEXICAN HAT, UT, USA

Aircraft #1

N75870

CESSNA T207A

Analysis

PLT STATED AFTER ACCIDENT THAT WHILE ON FINAL APPROACH WITH ENG PWR REDUCED FOR LANDING, THE ACFT BEGAN TO DESCEND BELOW THE DESIRED GLIDEPATH. WHEN THE THROTTLE WAS ADVANCED THERE WAS NO ADDED THRUST. AN IN-FLIGHT RESTART WAS UNSUCCESFUL. THE ACFT LANDED SHORT OF THE RUNWAY AN COLLIDED WITH A DIRT EMBANKMENT. POST CRASH FUNCTIONAL TEST OF THE ENG REVEALED NO EVIDENCE OF A MECHANICAL MALFUNCTION OR FAILURE THAT WOULD PRECLUDE NORMAL ENG OPERATION. THE ENG DID FAIL WHEN THE MIXTURE CONTROL WAS SET FOR SMOOTH ENG OPERATION, THE BOOST PUMP WAS IN THE OFF POSITION AND THE THROTTLE RAPIDLY ADVANCED FROM A LOW PWR SETTING TO FULL PWR.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports