Aviation Accident Summaries

Aviation Accident Summary ANC83LA138

MCGRATH, AK, USA

Aircraft #1

N1106Z

HUGHES 369D

Analysis

THE PLT STATED THAT HE WAS FLYING STRAIGHT & LEVEL AT APRX 700 FT AGL, WHEN THE ENG-OUT LIGHT ILLUMINATED. HE BEGAN AN AUTOROTATION TO A RIDGELINE. DURING THE LANDING, THE MAIN ROTOR BLADES CONTACTED THE TAIL BOOM & SEVERED IT FROM THE MAIN FUSELAGE. AN INVESTIGATION REVEALED THAT THE ENG BURNER DRAIN VALVE HAD AN AIR LEAKAGE OF 3000 CC/MIN. THE MAX ALLOWABLE OHM LIMIT WAS 800 CC/MIN (AT 20 PSI). THE COMBUSTION LINER HAD EXCESSIVE HEAT DISTORTION ADJACENT TO THE LARGE DIAMETER HOLE ON THE RIGHT SIDE OF THE SKIRT. THE 1ST STAGE TURBINE NOZZLE HAD SEVERE HEAT DISTRESS ON 14 TRAILING EDGE VANES & 11 LEADING EDGE VANES. THE FUEL NOZZLE HAD HEAVY CARBON DEPOSITS ON THE SPRAY TIP & AIR SHROUD. ALSO, A WHITE RESIDUE WAS FOUND IN THE ENG & A FUEL SAMPLE REVERSED 425 PARTS PER MILLION OF PHOSPHORUS.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports