Aviation Accident Summaries

Aviation Accident Summary FTW86MA030

DALLAS, TX, USA

Aircraft #1

N86SW

BOEING 737-2H4

Analysis

THIS INCIDENT OCCURRED WHEN THE NO. 2 ENGINE EXPERIENCED AN AFT ENGINE MOUNT CONE BOLT FAILURE AND THE SUBSEQUENT FAILURE OF THE SECONDARY SUPPORT LINK (STAINLESS STEEL CABLE). THE FAILURE OF BOTH AFT ENGINE SUPPORT ASSEMBLIES DURING THE TAKEOFF ROLL ALLOWED THE AFT SECTION OF THE ENG TO HANG DOWN TO WITHIN 4' OF THE GROUND. AS A RESULT, THE NO.2 THRUST REVERSER ACTUATOR ASSEMBLY DRUG THE RUNWAY ON ROTATION. IN ADDITION, ONE LEADING EDGE FLAP AND THE FORWARD ENGINE FAIRING WERE SLIGHTLY DAMAGED. THE ACFT SUBSEQUENTLY RETURNED TO THE ARPT AND LANDED WITHOUT FURTHER INCIDENT. METALLURGICAL EXAMINATION OF THE CONE BOLT REVEALED THAT IT FAILED AS A RESULT OF FATIGUE, MOST PROBABLY DUE TO IMPROPER INSTALLATION OF THE BOLT, SPECIFICALLY, THAT IT WAS UNDER TORQUED WHEN THE OPERATOR RE-INSTALLED THE ENG. THE SAFETY CABLE FAILED AS A RESULT OF OVERSTRESS, PROBABLY INDUCED WHEN THE ACFT ENCOUNTERED A ROUGH STRETCH OF RUNWAY DURING THE TAKEOFF ROLL.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports