Aviation Accident Summaries

Aviation Accident Summary ANC01LA055

FAIRBANKS, AK, USA

Aircraft #1

N3143A

Cessna 170B

Analysis

The commercial certificated pilot/flight instructor was conducting a local area instructional flight with the student pilot/owner of the airplane. The flight instructor reported that he was doing wheel landings with the student to a gravel runway. During the touch down on the third or fourth landing, the tailwheel assembly suddenly broke off. An FAA airworthiness inspector examined the airplane after the accident and found a preexisting crack in the tailwheel spring assembly that was about 1/16 inch deep, and about 1/2 inch long. The spring failed at the crack. When the tail wheel departed the airplane, it struck the bottom of the rudder, and the rudder trim tab. The bottom and aft portion of the rudder assembly was torn open. The spring assembly had accrued 126 hours, and 65 hours since the last annual inspection.

Factual Information

On May 7, 2001, at 1956 Alaska daylight time, a wheel-equipped Cessna 170B airplane, N3143A, sustained substantial damage during landing at the Fairbanks International Airport, Fairbanks, Alaska. The airplane was being operated as a visual flight rules (VFR) local area instructional flight when the accident occurred. The airplane was operated by the student pilot/owner. The commercial certificated pilot/flight instructor, and the student pilot, were not injured. Visual meteorological conditions prevailed. The flight originated at the Fairbanks International Airport at 1917. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), on May 9, 2001, the flight instructor reported that he was seated in the right seat, and was conducting wheel landings with the student on the ski strip, runway 19, at Fairbanks. During the touchdown on the third or fourth landing, the tailwheel assembly suddenly broke off. A Federal Aviation Administration (FAA) airworthiness inspector, Fairbanks Flight Standards District Office (FSDO), examined the airplane after the accident. He reported he found a preexisting crack in the tailwheel spring assembly that was about 1/16 inch deep, and about 1/2 inch long. He said the spring failed at the crack, and when the tailwheel departed the airplane, it struck the bottom of the rudder, and the rudder trim tab. The bottom and aft portion of the rudder assembly was torn open. In the Pilot/Operator Report (NTSB form 6120.1/2) submitted by the student pilot/owner, the owner indicated the tailwheel spring had a total time of 162 hours. The 6120.1/2 report noted an annual inspection was conducted on November 6, 2000, 65 hours before the accident.

Probable Cause and Findings

A failure of the tailwheel spring assembly due to fatigue during touch and go landings. A factor in the accident was an inadequate annual inspection by maintenance personnel.

 

Source: NTSB Aviation Accident Database

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