Aviation Accident Summaries

Aviation Accident Summary FTW01LA124

Raymondville, TX, USA

Aircraft #1

N7087X

Robinson R22

Analysis

The helicopter had been in flight for approximately 5 minutes when the main rotor rpm began to decrease. The "clutch light" illuminated and the "low rotor horn sounded." The pilot initiated an autorotation to an open field; however, he did "not have enough altitude" to clear some trees. The helicopter contacted the trees and impacted the ground "hard." The main rotor drive belts were found separated from the drive wheels. An examination of the helicopter by an aircraft mechanic and an FAA inspector revealed that the drive belts were "frayed and ripped." No anomalies were noted with the rest of the drive system. The helicopter was issued an airworthiness certificate on May 27, 1998. Review of the helicopter's maintenance records revealed that it had undergone its last annual inspection on February 10, 2001, at an aircraft total time of 409.2 hours. There was no record of the drive belts being replaced during the life of the helicopter. According to the helicopter manufacturer, the drive belts are to be changed on condition, and there is no life limit on the belts; however, the belts usually get replaced during the helicopter's 2,200-hour overhaul. At the time of the accident, the helicopter had accumulated a total of 488 hours.

Factual Information

On May 18, 2001, at 1000 central daylight time, a Robinson R22 helicopter, N7087X, was substantially damaged when it impacted trees and terrain following a loss of main rotor rpm while maneuvering near Raymondville, Texas. The commercial helicopter pilot and his pilot-rated passenger were not injured. The helicopter was registered to and operated by the pilot. Visual meteorological conditions prevailed and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The local flight departed a private ranch approximately 5 minutes prior to the accident. During a telephone interview conducted by the NTSB investigator-in-charge and in a written statement, the pilot reported that the helicopter had been in flight for approximately 5 minutes before the main rotor rpm began to decrease. The pilot stated that the "clutch light" illuminated and the "low rotor horn sounded." The pilot initiated an autorotation to an open field; however, he did "not have enough altitude" to clear some trees. The helicopter contacted the trees and impacted the ground "hard." According to the pilot and the FAA inspector, who responded to the accident, the helicopter sustained structural damage to the tail boom, the landing skids, and the horizontal stabilizer. The main rotor blades also sustained damage. The main rotor drive belts were found separated from the drive wheels. According to a written statement provided by an aircraft mechanic and the FAA inspector, the drive belts were found "frayed and ripped." No anomalies were noted with the rest of the drive system. The helicopter (serial number 2829) was issued an airworthiness certificate on May 27, 1998. Review of the helicopter's maintenance records revealed that it had undergone its last annual inspection on February 10, 2001, at an aircraft total time of 409.2 hours. At the time of the accident, the helicopter had accumulated a total of 488 hours. There was no record of the drive belts being replaced during the life of the helicopter. According to Robinson Helicopter Company, the drive belts should be replaced on condition, and there is no scheduled life limit for the belts; however, the belts usually get replaced during the helicopter's 2,200-hour overhaul.

Probable Cause and Findings

the failure of the main rotor drive belts while maneuvering which resulted in a loss of main rotor drive. A contributing factor was the lack of suitable terrain for the forced landing.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports