Aviation Accident Summaries

Aviation Accident Summary FTW02LA039

Galveston, TX, USA

Aircraft #1

N60TT

Piper PA-32-300

Analysis

The pilot had flown the airplane four days prior to the accident date, and after that flight, had inadvertently left the airplane's electrical master switch "ON," which resulted in a discharged battery. In order to start the engine, the pilot connected electrical power to the exterior battery receptacle. The pilot then boarded the airplane and started the engine. After the engine was started, the pilot "set the engine rpm to a low setting," got out of the airplane, and removed the exterior power source and wheel chocks. After removing the wheel chocks, the airplane started to move forward. The pilot attempted to stop the airplane, but was unsuccessful. Subsequently, the unoccupied airplane taxied across the airport into a wet field where it impacted a small ditch.

Factual Information

On November 15, 2001, at 1400 central standard time, a Piper PA-32-300 single-engine airplane, N60TT, was substantially damaged when it impacted a ditch while taxiing unoccupied at the Scholes Field Airport near Galveston, Texas. The instrument-rated private pilot, who was to be the sole occupant of the airplane, was not injured. The airplane was registered to and operated by the pilot. Visual meteorological conditions prevailed, and a flight plan was not filed for the proposed 14 Code of Federal Regulations Part 91 personal flight. In a telephone interview conducted by the NTSB investigator-in-charge, the pilot reported that he had flown the airplane four days prior to the accident date. The pilot stated that after that flight, he had inadvertently left the airplane's electrical master switch "ON," which resulted in a discharged battery. In order to start the engine, the pilot connected electrical power to the exterior battery receptacle. The pilot then boarded the airplane and started the engine. After the engine was started, the pilot "set the engine rpm to a low setting," got out of the airplane, and removed the exterior power source and wheel chocks. After removing the wheel chocks, the airplane started to move forward. The pilot attempted to stop the airplane, but was unsuccessful. Subsequently, the unoccupied airplane taxied across the airport into a wet field where it impacted a small ditch. An FAA inspector stated that a mechanic, who examined the airplane, reported the right main gear had collapsed damaging the wing spar. Numerous attempts to obtain a completed NTSB Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) from the pilot were unsuccessful.

Probable Cause and Findings

the pilot's failure to set the parking brake before exiting the aircraft to remove the wheel chocks.

 

Source: NTSB Aviation Accident Database

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