Aviation Accident Summaries

Aviation Accident Summary FTW82DA150

HOUSTON, TX, USA

Aircraft #1

N5784Y

AEROSPATIALE AS-350D

Analysis

THE PURPOSE OF THE FLIGHT WAS FOR THE PILOT TO PRACTICE MANEUVERS IN PREPARATION FOR A PART 135 CHECK RIDE. THE PILOT WAS PRACTICING POWER RECOVERY AUTOROTATIONS TO A HEIGHT OF ABOUT 5 FT AG. HE REPORTED THAT ON HIS FOURTH AUTOROTATION, THE ENGINE DID NOT ACCELERATE WHEN HE ATTEMPTED THE POWER RECOVERY. SUBSEQUENTLY, THE HELICOPTER FELL THROUGH THE RECOVERY AND LANDED HARD. DURING THE INVESTIGATION, THE ENGINE FUEL CONTROL AND POWER TURBINE GOVERNOR WERE REMOVED FOR EXAMINATION. THE GOVERNOR WAS FOUND TO BE WITHIN SPECIFICATIONS. HOWEVER, AN EXAMINATION OF THE FUEL CONTROL UNIT REVEALED THE PX TRIM BLEED PART WAS OVERSIZE. THE SPECIFICATION CALLED FOR A SIZE #64 TO #68 PART, BUT A #61 PART WAS INSTALLED. ALSO, THERE WAS SOME WEAR ON THE BELLOWS. ACCORDING TO BENDIX CORP, THE OVERSIZE PART AND WEAR WOULD HAVE LEANED THE MIXTURE, BUT WOULD NOT HAVE CAUSED THE POWER LOSS.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports