Aviation Accident Summaries

Aviation Accident Summary DEN03LA077

Sedan, NM, USA

Aircraft #1

N318BR

Air Tractor AT-502

Analysis

The pilot said the airplane refueling process took a very long time, due to the slow rate of fuel transfer. He drained 2 to 3 gallons of fuel from each tank to check for contamination. While descending from 1,200 feet to 150 feet agl, he looked down at a map on his lap to verify which field was to be sprayed. The pilot said the engine began losing power, dropping from 80 pounds of torque to 40 pounds of torque. He noticed the loss of power when he attempted to level off, and the airplane was near a stall. He dumped the chemical, and pushed the power lever full forward, with no increase in power noted. The pilot performed a forced landing straight ahead due to his low altitude, and impacted a rotating irrigation system in a wheat field. The airplane was substantially damaged. Postimpact examination revealed water in the fuel filters on the airplane's engine and on the refueling system. Water was also found in the airplane's right fuel tank and in the source fuel tank.

Factual Information

On April 24, 2003, at approximately 0930 mountain daylight time, an Air Tractor AT-502, N318BR, was substantially damaged when it collided with an irrigation system during a forced landing near Sedan, New Mexico. The commercial pilot received minor injuries. The airplane was being operated by Riddell Flying Service Inc., of West Helena, Arkansas, under the provisions of Title 14 CFR Part 137. Visual meteorological conditions prevailed for the local aerial application flight that originated from a private airstrip near Dalhart, Texas, at approximately 0910. No flight plan had been filed. Prior to departure, the airplane was serviced with fuel and chemicals. The pilot reported that after "about one hour and forty-five minutes [a very slow fuel transfer rate]" both fuel tanks were filled to capacity. He said the fuel was "flowing extremely slow." The pilot stated he drained 2 to 3 gallons of fuel out of each tank to check for contamination before departing. While descending from 1,200 feet to 150 feet agl, the pilot looked down at a map on his lap to verify which field was supposed to be sprayed. The pilot said the engine (a Walther STC conversion) began losing power, dropping from 80 pounds of torque to 40 pounds of torque. He noticed the loss of power when he attempted to level off, and the airplane was near a stall. He dumped the chemicals, and pushed the power lever full forward, with no increase in power noted. The pilot performed a forced landing straight ahead due to his low altitude, and impacted a rotating irrigation system in a wheat field. The top of the hopper was crushed, and the canopy and its supporting structure were destroyed. The pilot received facial cuts, shoulder abrasions, and a broken thumb. Postimpact examination revealed water in the engine fuel filters and in the refueling system. An examination of the airplane systems revealed no anomalies. A few days after the accident, the manager of Air Service went to pump off the Jet A from the fuel tanks in the airplane, and he found approximately 6 ounces of water in the right fuel tank. He also checked the tank that the airplane was fueled from, and he found approximately 5 inches of water in that tank. The engine was test run at the operators facilities in Helena, Arkansas, and no abnormalities were noted.

Probable Cause and Findings

the nonmechanical partial loss of engine power due to water contamination of the fuel. Contributing factors include the lack of suitable terrain for a forced landing (due to his low altitude), and the irrigation system (object) that was impacted.

 

Source: NTSB Aviation Accident Database

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