Aviation Accident Summaries

Aviation Accident Summary LAX03IA259

Honolulu, HI, USA

Aircraft #1

C-FYKX

Airbus A340-300

Analysis

Both of the transport airplane's center landing gear tires (#'s 9 and 10) shredded during takeoff roll, damaging the door retraction arms and multiple fuselage skin panels. The flight crew could not retract the landing gear and elected to return to the departure airport and performed an uneventful overweight landing. Examination of the tire debris revealed there was significant inter ply tearing of the tires, suggesting the tire did not fail as a result of a cap failure. According to the operator and tire manufacturer, the failure signatures were consistent with a rapid and violent event, which can be attributed either to foreign object damage (FOD) or a low tire pressure situation. Since the #10 tire exhibited high heat signatures, the likely sequence is that the #9 wheel tire failed first, followed by the overheating of the #10 tire and its subsequent failure. The fact that no FOD was recovered with the tire debris and the fact that the nose tires did not sustain any damage, considering their in-line position with the center landing gear, lends more credence to the low tire pressure situation. The airplane underwent a regularly scheduled service check, which included a tire condition and pressure check, approximately 30 hours prior to the event. The tire pressure was not documented during the service check. A post-incident examination revealed the #9 wheel had a leaking fuse plug. The fuse plug was tested and found to have a 6-psi leak over a 12-hour time period. The pre-incident tire pressure was unknown.

Factual Information

HISTORY OF FLIGHT On August 18, 2003, at 0316 Hawaiian standard time (HST), an Airbus Industrie A340-300 transport category airplane, Canadian registration C-FYKX, sustained minor damage when its center landing gear tires shredded on takeoff roll from the Honolulu International Airport, Honolulu, Hawaii. The captain, first officer, relief pilot, 10-cabin crew, and 172 passengers were not injured. The airplane was operated by Air Canada of Quebec, Canada, as flight 33 under the provisions of 14 CFR Part 129 international operations. The international flight departed Honolulu and was destined for Sydney, Australia. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed. According to the captain, who was the non-flying pilot, the engine start and taxi for takeoff were normal, and the brake temperatures were considered low for the long taxi. The flight taxied to runway 8R and started its takeoff roll. When the airplane reached approximately 100 knots the flight crew felt a slight vibration similar to that felt with a slight nose gear shimmy and/or rough runway. The rotation (approximately 155 knots) was described as smooth. When the landing gear handle was placed to the retracted position, the flight crew received a LGCIU (Landing Gear Control and Interface Unit) #2 fault indication on the EICAS (Engine Indicating Crew Alerting System). The flight crew heard wind noise around the airplane and knew the landing gear doors were not retracted. The first officer (flying pilot) flew the airplane along its departure course and they contacted air traffic control and informed them the airplane was experiencing landing gear problems. When the airplane passed through 1,500 feet, the flight crew viewed the wheel condition page on the EICAS and noted that all of the landing gear doors were open. The checklist was referenced and indicated that the landing gear should be recycled down then up again. When the crew placed the landing gear handle to the down position they received an indication the landing gear were down and locked and the landing gear doors were closed. When the crew placed the landing gear handle back to the retracted position, they received the same LGCIU #2 fault. After that, they reset the LGCIU #2 circuit breaker, but did not note a change in the system. The flight crew contacted their dispatch, informed them of the problem, and elected to return to Honolulu. They elected to conduct an overweight landing on runway 8L (the longest runway) and obtained a landing gear down and locked indication before landing. The landing was uneventful until the airplane decelerated to approximately 50 knots. That's when the flight crew obtained a LGCIU #1 fault along with the LGCIU #2 fault. The loss of the #1 system eliminated the nose wheel steering. The captain directed the airplane off runway 8L onto runway 4L, where the airplane came to a stop. Maintenance personnel met the airplane on runway 4L and informed the flight crew of the damage to the center landing gear tires and landing gear doors. Airport personnel brought stairs out to the airplane and the passengers and crews deplaned the airplane and were driven to the terminal area. According to the flight crew, the cabin crew did not report hearing any loud bangs or pops, but did notice the noise of the tire debris impacting the airplane belly. AIRCRAFT INFORMATION The aircraft was equipped with this centerline landing gear to permit operation with an increased maximum certified operating weight of 271,000 kilograms. For the occurrence flight, the take-off weight was about 240,900 kilograms. The centerline landing gear is a forward-retracting gear that incorporates a mechanical downlock and an airframe-mounted uplock. It is positioned under the center of the fuselage and directly in line with the rear wheels on the left and right main landing gear bogies. The centerline landing gear's primary purpose is to carry a share of the aircraft weight on the ground so as to not overload the main landing gear. The center landing gear consists of two wheels (#9 and #10) positioned side-by-side on one axle, each utilizing a 36-ply, tubeless tire. The center landing gear does not utilize brakes. The tire for wheel #9 was manufactured by Goodyear Aviation and was retread on two previous occasions, as marked by the R-2 on its sidewall; its last retread taking place in March 2003. The tire for wheel #10 was also manufactured by Goodyear and was retread on three previous occasions; the last retread taking place in April 2003. On August 16, 2003, at 1900 HST, the aircraft underwent a regularly scheduled service check in Vancouver, British Columbia, Canada. The service check required that the tire condition and pressure be checked. According to the service check checklist, the center wheel tire pressure should be between 158 and 166 pounds per square inch (psi). The checklist does not require the checked tire pressure to be noted. The checklist does indicate that if a tire is found under-inflated, a "maintenance snag" is to be entered into Air Canada's line maintenance computer system. The maintenance snag is to be "monitored," and if the tire is found to be under-inflated again during the next service check, the wheel is to be removed and replaced. If the tire is found to be within the tire pressure limits at the next service check, the maintenance snag is to be removed. Review of the maintenance records for the incident airplane revealed no open maintenance snags relating to the center landing gear tire servicing. WRECKAGE AND IMPACT INFORMATION Airport personnel searched both runway 8R and 8L for tire debris. Approximately 80% of the tires were found on both runways; however, the departure runway contained the majority of the debris. The Goodyear tire beads remained attached to their wheels, but the wheel plies and retread was destroyed and shredded. The left wheel displayed more peening damage to its outboard edge than the right wheel. The left wheel also displayed more heat signatures on the bearing access cover than the right wheel. The center landing gear sustained damage to its left and right wheels, the left aft door retraction arm, and the aft center door retraction arms. Numerous belly panels were punctured and numerous panel supports were bent. The tire remnants were shipped back to Air Canada for further examination by Air Canada and Goodyear personnel. TESTS AND RESEARCH Examination of the tire debris revealed the casing and cap for both tires were shredded. Only the bead and portions of the sidewall remained on each wheel. The tire segments were sorted out by using characteristics such as discoloration, side markings, and shape. The #10 wheel tire segments were very blue, which is an indication of the tire at one time being very hot (oil "sweating" out of the rubber). The #10 tire broke up into many pieces varying in size. The #9 tire was not discolored out of the ordinary, and it broke up into primarily large pieces. The majority of the tire segments for both the #9 and #10 tires included various sizes of caps and casings. The thickness of the tread pieces ranged from one fabric ply in width to the entire thickness of the tread/casing/liner. Some of the large tread pieces are diamond shaped (or similar to an X-type pattern), which according to Goodyear and Air Canada, suggested a "rapid failure mode." Goodyear's analysis of numerous retread/casing interfaces, indicates that the retread package adherence to the surrounding casing was "excellent for both tires," and there was "no obvious workmanship issues with either tire." The wheel fuse plugs were tested for leaks and one of the fuse plugs off of wheel #9 was found to leak. To quantify the degree of leak, the leaking fuse plug was installed on a serviceable Airbus A340 main wheel/tire assembly and inflated to full operating pressure (210 psig). The serviceable assembly was allowed to stabilize, and after 12 hours, a 6-psi drop was noted. This was considered to be a moderate leak, but within serviceable limits. Assuming the leaking fuse was leaking at the rate tested, the tire pressure would have dropped approximately 15 psig since the last service check, which took place approximately 32 hours prior to the event. The failure descriptions mentioned above were consistent with that of a rapid failure. According to Goodyear and Air Canada, the two likely scenarios leading to this type of failure is a foreign object damage (FOD) situation, or a low tire pressure situation. It should be noted that no FOD was collected with the tire debris from the runway, and no damage was sustained by the nose landing gear, which is in line with the center landing gear.

Probable Cause and Findings

the failure of the center landing gear tires as a result of low tire pressure.

 

Source: NTSB Aviation Accident Database

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