Aviation Accident Summaries

Aviation Accident Summary DEN04IA012

Denver, CO, USA

Aircraft #1

N375FE

McDonnell Douglas DC-10-10

Analysis

According to the captain, during the take-off roll, and shortly after the first officer called out the take-off decision speed (V1,158 knots), the take-off warning horn sounded. At that time, the captain initiated a Rejected Take-Off (RTO). Assured that a stop on the runway was possible, he elected not to apply maximum braking in "hopes that a more gentle brake application might avoid or mitigate any damage to the aircraft and lessen the heat and fire risk." During the RTO, DEN tower contacted the crew and reported smoke in the vicinity of the left main landing gear. Immediately thereafter, the tower reported that fire was coming from the same area. DEN tower initiated a call to alert aircraft rescue and firefighting equipment (ARFF) to the scene. The aircraft came to a stop, on the runway centerline, with approximately 1,800 feet of runway remaining. The crew completed the emergency quick evacuation checklist, and all seven persons aboard egressed via the L1 escape slide. The initial inspection of the airplane revealed that both of the nose landing gear tires, two main landing gear brake lines, all eight main landing gear brake assemblies, and all eight main landing gear tires were damaged during the RTO. Each damaged item was required to be replaced prior to towing the aircraft off the runway. The maintenance manager stated that the nose and main landing gear assemblies had "overheated," during the RTO and that each tire had deflated after the airplane came to rest, because "there was no indication that the tires had skidded." During an examination of the airplane, it was determined that the take-off warning horn was the result of a take-off configuration conflict between the inboard and outboard slats. An inspection of the inboard slat drive mechanism's lower left hand anti-torque strut, revealed that a rod-end bearing had migrated out of the rod-end, and that two washers were missing, which allowed the anti-torque strut to ride on the bolt that attaches the rod-end to the slat drive mechanism.

Factual Information

HISTORY OF FLIGHT On October 12, 2003, at 0717 mountain daylight time, a McDonnell Douglas DC-10-10, N375FE, owned by Federal Express Corporation, Memphis, Tennessee, and operating as FedEx flight 840, sustained minor damage during a rejected takeoff at Denver International Airport (DEN), Denver, Colorado. The airline transport certificated captain, airline transport certificated first officer, flight engineer, and four non-revenue passengers were not injured. Visual meteorological conditions prevailed. An instrument flight rules (IFR) flight plan was filed for the scheduled domestic cargo flight being conducted under the provisions of Title 14 CFR Part 121. The flight to Memphis, Tennessee, was originating at the time of the accident. According to a Federal Express representative, at 0646, flight 840 "blocked out" from the FedEx ramp at DEN for a direct flight to Memphis. The aircraft taxied approximately 6 miles, and at 0717 it was cleared for take-off on runway 16R (16,000 x 200 feet). According to the captain, during the take-off roll, and shortly after the first officer called out the take-off decision speed (V1, 158 knots), the take-off warning horn sounded. At that time, the captain initiated a Rejected Take-Off (RTO). Assured that a stop on the runway was possible, he elected not to apply maximum braking in "hopes that a more gentle brake application might avoid or mitigate any damage to the aircraft and lessen the heat and fire risk." During the RTO, DEN tower contacted flight 840 and reported smoke in the vicinity of the left main landing gear. Immediately thereafter, the tower reported that fire was coming from the same area. DEN tower initiated a call to alert aircraft rescue and firefighting equipment (ARFF) to the scene. The aircraft came to a stop on the runway centerline at the D3 intersection. Approximately 1,800 feet of runway remained. After completing the emergency quick evacuation checklist, all seven persons aboard egressed via the L1 escape slide. At 0725, the tower closed the runway to all operations. According to a FedEx field line maintenance manager, the initial inspection of the airplane revealed that both of the nose landing gear tires, two main landing gear brake lines, all eight main landing gear brake assemblies, and all eight main landing gear tires were damaged during the RTO. Each damaged item was required to be replaced prior to towing the aircraft off the runway. The maintenance manager stated that the nose and main landing gear assemblies had overheated, during the RTO. He stated that each tire must have deflated after the airplane came to rest, because "there was no indication that the tires had skidded." Each wheel on the left main landing gear assembly (number 1, 2, 5, and 6), was "welded" to its brake assembly. Between each "welded" tire and brake assembly was also an axial spacer that is normally reused during tire replacement. Due to the lack of replacement parts being on hand, replacement tires, brake lines, and spacers were flown in from other locations. The damaged items were replaced and the airplane was towed to the FedEx ramp. The runway was cleared and reopened at 0038 the following morning. TEST AND RESEARCH According to Flight Data Recorder (FDR) information, during the take-off roll and subsequent RTO, the right outboard (ROB) slats went from take-off (TO) to landing (LAND) configuration at 156 knots and returned to TO configuration at 152 knots. During this same time, the left outboard (LOB) slats went from TO to LAND configuration at 164 knots and returned to TO configuration at 162 knots. According to a FedEx systems engineer, this condition would result in the activation of the "take-off warning horn because the slats are no longer in take-off configuration." During an examination of the airplane, it was determined that the take-off warning horn was the result of a take-off configuration conflict between the inboard and outboard slats. An inspection of the lower left hand anti-torque strut (p/n ARH0518-1, IPC 27-83-05-01 item 534), revealed that it had separated from its attachment point on the inboard slat drive mechanism. Upon further inspection, it was noted that a rod-end bearing (p/n MS21232-9), had migrated out of the rod-end (p/n ARH0514-1), and that the two required washers (p/n S2431218-9S20G, CPN 5711588), were missing. This allowed the anti-torque strut to ride on the bolt that attaches the rod-end to the slat drive mechanism. An initial inspection of the bearing revealed that the bearing had migrated out of the rod-end under "axial loads" and that the bearing was "never staked." Further examination revealed that whether the bearing was properly staked or not, the bearing migrated out of the rod-end because the washers were not properly installed. There had been no prior repair or maintenance history pertaining to this component and this was the first time the strut had been removed from the airplane. On October 20, 2003, a FedEx maintenance engineer examined the left and right wheel and brake assemblies. He stated that the left main landing gear brakes appeared to have been exposed to higher heat, due to a "high energy stop," which caused the wheels and brakes to fuse together. Although several tires received heat damage due to the "hot brakes and tire rims contacting the [tire] side walls," the general observation was that the tires had deflated after the airplane came to a stop. The left main landing gear brakes (number 5 and 6), and the aft inboard and outboard brake hoses were damaged by excessive heat. He stated that the tires did not exhibit any signs of "skid-thru" or damage due to rolling while flat. Although there was extensive heat damage to the wheel and brake assemblies, no wheel or brake deficiencies were noted. ADDITIONAL INFORMATION According to the captain, FedEx flight 840 was originally a non-stop flight from Oakland, California, to Memphis, Tennessee. During the flight, the captain was directed to divert to Denver to pick up additional freight. The additional freight and fuel resulted in a calculated take-off gross weight of approximately 404,900 pounds, and a landing-limited operational maximum take-off gross weight of approximately 406,700 pounds. The captain said that he anticipated a departure on runway 17R until he noticed that the airplane had been over fueled by approximately 400 pounds. Due to the extra fuel and the reports of wind shear from DEN tower, he elected to taxi to runway 16R to taxi off the over-fuel weight and take advantage of the longer runway. On November 18, 2003, FedEx issued a Fleet Campaign Directive (FCD), 8-27-040 A, which required the inspection of the inboard slat drive mechanism and the lower left and right hand anti-torque struts for the proper washer installation and staking of the rod-end bearing. The FCD required the inspection of all DC-10, MD-10, and MD-11 aircraft. According to Douglas Aircraft Company (DAC) CMM 27-83-14, the rod-end bearing (p/n MS21232-9), is to be staked in the rod-end per Douglas Process Specifications (DPS) 1.33-2.

Probable Cause and Findings

the manufacturer's improper installation of the inboard slat drive mechanism's lower left hand anti-torque strut, which resulted in the axial migration of the rod-end bearing, the binding of the anti-torque strut, and the subsequent activation of the slat take-off configuration warning horn. Contributing factors include the aborted take-off, the initiation of normal brakes during a high energy stop, and the main landing gear fire.

 

Source: NTSB Aviation Accident Database

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