Aviation Accident Summaries

Aviation Accident Summary CHI04LA146

Prosser, NE, USA

Aircraft #1

N731MP

Cessna A188B

Analysis

The airplane was substantially damaged and the pilot was fatally injured when the aircraft inadvertently stalled, began a spin, and impacted terrain during a maneuver to avoid a transmission tower. The owner/operator of the accident aircraft reported that the pilot was completing a period of training prior to being hired at the operator's agricultural application service. During the accident flight the pilot was to complete ten practice application passes. The operator stated that he witnessed the takeoff, however, instead of turning out to the east, the pilot turned to the west. The operator noted that he drove to the designated practice field, but the accident aircraft never arrived. A witness reported that the aircraft was flying about 500 feet above ground level, when it suddenly banked hard and appeared to go straight down. A second witness reported that he did not see the aircraft in flight, but looked up to see the impact. This witness stated he "saw the moment of impact and it appeared to have gone [straight] down into the ground." A transmission tower, extending 625 feet above ground level, was located approximately 1,000 feet south of the accident site. Flight control continuity was established from the control surfaces to the cabin area during a post-accident examination.

Factual Information

HISTORY OF FLIGHT On June 21, 2004, at 1013 central daylight time, a Cessna A188B, N731MP, operated by Muckels Aerial Inc. and piloted by the commercial pilot, was substantially damaged during an in-flight collision with terrain near Prosser, Nebraska. The aerial application training flight was being conducted under 14 CFR Part 91 without a flight plan. Visual meteorological conditions prevailed. The pilot sustained fatal injuries. The local flight departed Aknux Airport (NE38), Prosser, Nebraska, about 1000. The owner/operator of the accident aircraft reported that the pilot was completing a period of training prior to being hired at the operator's agricultural application service. During the accident flight, the pilot was to complete ten practice application passes to a field east of NE38. After the practice runs the pilot was to become familiar with the local area and return to the departure airport. The operator stated that he witnessed the takeoff, however, instead of turning out to the east, the pilot turned to the west. The operator noted that he drove to the designated practice field, but the accident aircraft never arrived. A witness to the accident reported that the aircraft was flying west, approximately 500 feet above ground level (agl), when it suddenly banked hard to the north and appeared to go straight down. He commented that "no noticeable debris detached from the aircraft" and that it appeared to be intact as it went down. A second witness reported that he did not see the aircraft in flight, but looked up to see the impact. He stated he "saw the moment of impact and it appeared to have gone [straight] down into the ground." A third witness reported that he saw the aircraft flying in a southeast-to-northwest direction. The aircraft banked hard and started to turn toward the north. He commented that the aircraft appeared to be intact. He noted that he did not see the impact. The main wreckage was determined to be located at 40 degrees 44.12 minutes north latitude, 098 degrees 34.30 minutes west longitude, using a handheld global positioning system (GPS) receiver. The accident site was located about 1-1/2 miles north-northwest of NE38. The entire debris area was within approximately 50 feet of the main wreckage. A transmission tower was located approximately 1,000 feet south of the accident site. The tower height was listed at 625 feet agl on the Omaha sectional chart. A post-accident inspection of the airplane was conducted. All flight control surfaces remained attached to the aircraft. Flight control continuity was established from the control surfaces to the cabin area. PERSONNEL INFORMATION The pilot held a commercial pilot certificate with single-engine land and instrument airplane ratings. According to Federal Aviation Administration (FAA) records the certificate was issued on May 1, 2004. The pilot held a second-class airman medical certificate with no limitations issued on July 26, 2004. A copy of the pilot's logbook was obtained and reviewed. Total logged flight time was 276.4 hours. The logbook included endorsements for training and proficiency in the operation of complex and high performance airplanes. These endorsements were dated April 23, 2004. The most recent entry was dated June 15, 2004. This flight consisted of 1.6 hours dual instruction in a Piper PA-18 airplane. The remarks column noted, "spray practice" for this flight. The accident pilot had completed a course of agricultural pilot training on May 3, 2004. According to documentation provided by the course operator, the agricultural training consisted of approximately 40 hours of flight time. Topics reportedly covered during the course included full gross weight takeoffs and landings, field entries and departures, and obstacle clearance. The accident pilot received additional training in preparation for the FAA commercial pilot practical test concurrent with the agricultural application training. AIRCRAFT INFORMATION The accident airplane was a 1977 Cessna A188B Ag Truck, serial number 18803003T, certified under FAA Type Certificate A9CE. This was a single-engine, single-place, restricted category, airplane approved for agricultural application operations. The airplane was originally certified with a Continental IO-520-D, 300 horsepower engine. The accident airplane was subsequently modified to install a Lycoming IO-720-A1B (serial number L-1551-54A), 400 horsepower engine. The modification was authorized under FAA Supplemental Type Certificate (STC) SA3609SW. The installation on the accident airplane was approved on July 17, 2002, and documented on FAA Form 337, Major Repair and Alteration. An annual inspection was completed on March 2, 2004, at an airframe total time of 2,764.9 hours. According to the logbook, the recording tachometer indicated 382.6 hours at the time of the annual inspection. The tachometer indicated 480.5 hours at the accident site. METEOROLOGICAL INFORMATION Weather conditions recorded by the Hastings Municipal Airport (HIS) Automated Surface Observing System (ASOS), located 9 miles southeast of NE38, at 0953, were: scattered clouds at 11,000 feet agl; winds from 320 degrees at 13 knots; and 10 miles visibility. ADDITIONAL INFORMATION The FAA and Cessna Aircraft Company were parties to the investigation.

Probable Cause and Findings

The pilot's abrupt maneuver to avoid obstructions, and his failure to maintain adequate airspeed resulting in a stall. The low altitude flight operation, and the transmission tower (antenna) were contributing factors.

 

Source: NTSB Aviation Accident Database

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