Aviation Accident Summaries

Aviation Accident Summary SEA04LA145

Louie Lake, ID, USA

Aircraft #1

N277LF

Bell 222U

Analysis

After the medical evacuation flight arrived at its designated landing zone (6,500 feet mean sea level/MSL), an out-of-ground-effect hover was accomplished to verify the aircraft's performance. The power check was good and a positive rate of climb was noted. After landing and the crew had exited the aircraft, the pilot departed the area to locate a landing zone closer to the pickup point of the crew and patient. A landing zone at the 6,600 foot level (MSL) was located 3/8 of a mile closer to the patient pickup point. While waiting to load the patient the pilot determined a takeoff could be made based on his review of the aircraft's takeoff performance data. After completing an in-ground-effect power check and initiating a vertical climbout, the pilot confirmed the helicopter would clear a 100 foot tree line as it began to transition forward. After clearing the tree line the pilot detected the aircraft lose all lift as the helicopter began to settle toward the approaching trees. Applying the remaining power, the RPM warning sounded, prompting the pilot to reduce collective, but only to realize that he was descending into approaching obstacles. Right pedal was applied in an attempt to return to the original point of departure, however, the rotor RPM had still not completely recovered and the aircraft continued to descend. The aircraft impacted a boulder, and with the RPM now fully recovered, the helicopter jumped back into the air. The aircraft then rotated 180 degrees before the pilot performed a hover autorotation. During the maneuver the tail rotor had impacted a tree branch which resulted in an 8 inch chord wise gash to one of the tail rotor blades. The pilot felt that as the helicopter was clearing the tree line it entered a downwind condition, a condition which he didn't anticipate, resulting in a reduced power margin with which to overcome the loss of lift. A weather reporting station located 7 miles west-northwest of the accident site reported the wind was variable at 3 knots. The density altitude was calculated to be 8,898 feet. The pilot did not assert that any mechanical malfunctions precipitated the accident.

Factual Information

On July 14, 2004, approximately 1220 mountain daylight time, a Bell 222U helicopter, N277LF, was substantially damaged while maneuvering during departure from Louie Lake, Idaho. The helicopter was registered to PNC Leasing LLC of Pittsburgh, Pennsylvania, and operated by CJ Systems Aviation Group, Inc., of West Mifflin, Pennsylvania. The commercial pilot, flight nurse, paramedic, and patient who was being transported were not injured. Visual meteorological conditions prevailed for the 14 CFR Part 135 medical evacuation flight, and a flight plan was not filed. The flight was originating at the time of the accident. In a written statement provided to the NTSB investigator-in-charge (IIC), the pilot reported that upon arrival at the designated landing zone (LZ), located 6,500 feet above mean sea level (MSL), "I told the crew we were going to perform an out-of-ground-effect (OGE) hover to verify the aircraft performance. The power check was good and we had a positive rate of climb OGE." The pilot reported that after landing and deplaning the crew, he decided to depart the LZ to locate another one which would be closer to the patient/crew pickup point. The pilot further reported locating an LZ about 3/8 of a mile closer to the pickup point at 6,600 feet MSL. The pilot stated that while waiting for the crew to load the patient he determined the passenger's weight, computed the [aircraft's] weight and balance, and checked his performance charts. The pilot reported, "Everything checked out fine and the patient was loaded. The crew checklist was completed and I performed [an] IGE (in-ground-effect) power check. All systems looked good and we departed at approximately 1220 hours." The pilot stated the aircraft performed well during the vertical climbout and he could see the helicopter would clear the 100 foot tree line as it began to transition forward. "As the rotor system cleared the tree line and forward progress was started, I felt the aircraft lose all lift and begin to settle back toward the approaching trees. I applied the remaining power that I had left." The pilot reported the audible RPM warning sounded, accompanied by a slight yaw. The pilot stated, "I reduced collective, realized I was descending into my obstacles, and essentially performed a quick stop, applied right pedal and attempted to return to the original point of departure." The pilot further stated that the rotor RPM had still not completely recovered at this point. "I attempted to cushion the impact with collective and we touched down in the confined area with zero ground speed." The pilot reported the left skid impacted a boulder, the RPM fully recovered, and the aircraft "jumped" back into the air. The pilot further reported, "We rotated 180 degrees [and] I responded by rolling the throttles off and performed a hover autorotation. [After landing] I performed the emergency shutdown and we evacuated the patient." The pilot further stated that there were several boulders where the helicopter impacted the terrain, and that the left skid tube between the crosstubes was broken. The pilot also reported that during the 180 degree rotation the tail rotor contacted a tree branch and damaged a tail rotor blade. The pilot stated that at the departure point the wind was calm and was shielded with tall tress. The pilot related, "It is my feeling that as I cleared the tree tops I entered a downwind condition. I did not anticipate this downwind condition and did not have enough of a power margin to overcome this loss of lift. The pilot did not assert that any mechanical malfunctions precipitated the accident. According to a Federal Aviation Administration (FAA) inspector, who conducted a post accident examination of the tail rotor, the helicopter had sustained an approximately 8 inch chordwise gash to one of the tail rotor blades as a result of the impact with the tree branch. According to the Pilot/Operator Aircraft Accident Report provided to the IIC, weather conditions at the accident site were reported to be wind from the southeast at 10 knots with gusts to 10 knots, ceiling and visibility unlimited, temperature 70 degrees Fahrenheit, and an altimeter setting of 29.91 inches of Mercury. At 1250, the McCall Municipal Airport (MYL) Automatic Surface Observing System (ASOS), located 7 nautical miles west-northwest of the accident site elevation 5,021 feet MSL, reported wind variable at 3 knots, visibility 10 statute miles, sky clear, temperature 84 degrees Fahrenheit, dew point 48 degrees Fahrenheit, and an altimeter setting of 30.08 inches of Mercury. Density altitude at the accident site was calculated to be 8,898 feet.

Probable Cause and Findings

The failure of the pilot to maintain rotor rpm and his inadequate recovery from a bounced landing. Factors contributing to the accident included the tailwind condition and the tree.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports