Aviation Accident Summaries

Aviation Accident Summary ATL04LA171

Dayton, TN, USA

Aircraft #1

N1209J

Hawkins William Searey

Analysis

According to the certified flight instructor, while practicing a series of glassy water landings. On the eight landing while on step the airplane pitched down violently and the airplane flipped over nose first, and came to rest inverted. According to the second pilot, after touchdown on the river, while on the step traveling at approximately 40 mph the nose of the airplane "jerked downward". The airplane then violently pitched down under the water, and the cockpit filled with water. No flight control or mechanical problems were reported by the pilot's prior to the accident. Examination of the airplane revealed that the hull of the airplane was delaminated. The nose of the airplane separated from the airframe assembly.

Factual Information

On August 26, 2004, at 2000 central daylight time, a William Searey experimental airplane, N1209J, registered to and operated by a private owner, nosed over during a water landing on the Hiawassee River, Dayton, Tennessee. The instructional flight was operated under the provision of Title 14 CFR Part 91 with no flight plan filed. Visual meteorological conditions prevailed at the time of the accident. The experimental airplane sustained substantial damage. The certified flight instructor (CFI) and private pilot reported minor injuries. The flight departed Dayton, Tennessee, on August 26, 2004 at 1900. According to the CFI, while they were practicing a series of glassy water landings, and while on the step of the eight landing, the airplane "pitched down violently" and nosed over into the water and sank. According to the private pilot, after touchdown on the river, while on the step traveling at approximately 40 mph, the nose of the airplane "jerked downward". The airplane then violently pitched down under the water, and the cockpit filled with water. No flight control or mechanical problems were reported by the pilot's prior to the accident. The post-accident examination of the airplane revealed that the forward section of the nose was missing, and the hull was delaminated. The forward bulkhead and stringers of the hull were made with lumber with multiple knots in the wood, and some evidence of pitch. There was low adhesion of fiberglas to the bulkhead and stringers. Fibers were broken away from the bulkhead and stringers revealing low adhesion to the wood supportive structure. The examination of the fiberglas hull also disclosed evidence of air voids under the bi-directional bonded fiberglas. Review of the maintenance records revealed that the airplane had an annual inspection on June 7, 2004, and had accumulated a total time in service of 143.7 flight hours. The airplane received its special airworthiness certificate on December 17, 1996, and completed its flight test hours on September 21, 1997.

Probable Cause and Findings

The delamination of the fiberglass hull of the airplane.

 

Source: NTSB Aviation Accident Database

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