Aviation Accident Summaries

Aviation Accident Summary SEA05LA128

Madras, OR, USA

Aircraft #1

N555TE

Ellsberg One Design

Analysis

The pilot was practicing aerobatic maneuvers in the single-seat experimental airplane when the accident occurred. Witnesses observed the pilot make a low pass down the runway and then enter a vertical ascent. The airplane climbed to about 1,500 feet agl, at which point the pilot placed the airplane in a flat spin. After completing 4 to 5 rotations, the pilot recovered from the spin. The witnesses estimated that after the spin recovery, the airplane was at an altitude between 70 and 200 feet agl. The airplane continued to descend, impacted the ground, exploded and was consumed by fire. An on scene examination of the wreckage by an FAA inspector found no evidence of any pre-impact mechanical discrepancies.

Factual Information

On June 25, 2005, about 1333 Pacific daylight time, an Ellsberg One Design amateur-built experimental airplane, N555TE, impacted the ground during performance of aerobatic maneuvers at the City-County Airport near Madras, Oregon. The commercial pilot, the sole occupant, sustained fatal injuries, and the airplane was destroyed by impact and fire damage. The airplane was registered to and operated by the pilot. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that was conducted under 14 CFR Part 91. The airplane departed from the Madras Airport at an unknown time. According to a report by an officer with the Jefferson County Sheriff's Office who responded to the scene of the accident, the pilot was a "featured stunt pilot in the yearly Madras air show" and was practicing aerobatic maneuvers when the accident occurred. According to a written statement provided by a witness, who was standing outside a hangar on the airport observing the flight, the pilot made his third pass "to the North paralleling runway 34 on the east side of the asphalt and transitioned into a vertical climb, [and] at the top of the climb at an altitude of approximately 1500 [feet] AGL he put the aircraft into a controlled flat spin to the left." The witness reported that the pilot completed 4 to 5 rotations before recovering from the spin "on a heading towards the south at an altitude of about 70 feet AGL." The witness further reported that "at this point it appeared that the pitch was lowered to approximately -15 degrees at around 40 feet AGL but for a very short amount of time and very little forward speed was gained. At around 20 feet AGL it appeared that the pitch was increasing, but not arresting the vertical descent. The aircraft impacted the ground and immediately erupted in flames." According to a written statement provided by another witness, who was standing next to the first witness, the pilot made a high speed low level pass over the runway at about 60 feet agl and then pulled up, climbing to about 1,500 feet agl. The pilot then put the airplane into a flat spin and completed 4 to 5 rotations. At about 200 feet agl, the pilot recovered from the spin. According to the witness, "after his dive recovery it looked like he didn't have enough speed and pulled up and stalled and pitched forward and down and impacted at about [a] 45 degree angle and exploded on impact." An FAA inspector conducted an on scene examination of the wreckage and did not report finding evidence of any pre-impact mechanical discrepancies. The inspector reported that there was a ground scar approximately 10 feet long leading to the wreckage and that the airplane was consumed by fire with the exception of the steel frame fuselage and the engine. FAA records indicated that the pilot was the builder of the single-seat experimental airplane, which was issued its airworthiness certificate and operating limitations on September 11, 1996. According to a friend of the pilot, he had flown the airplane about 900 to 1,000 hours. The airplane's maintenance logbooks were not located during the investigation. The pilot held a commercial pilot certificate and a flight instructor certificate with single engine land and instrument ratings on both certificates. His most recent second class medical certificate was issued on February 19, 2005. On the application for this medical certificate, the pilot reported a total flight time of 4,000 hours and a flight time in the last six months of 150 hours. The pilot's flight logbooks were not located during the investigation. An autopsy of the pilot was performed by the Medical Examiner Division of the Oregon State Police in Clackamas, Oregon. Toxicology tests were performed by the FAA's Toxicology and Accident Research Laboratory. The tests were negative for drugs. Ethanol was detected in muscle. The toxicology report stated that "the ethanol found in this case is from sources other than ingestion."

Probable Cause and Findings

The pilot's failure to maintain altitude/clearance from terrain while performing aerobatics which resulted in a collision with the ground.

 

Source: NTSB Aviation Accident Database

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