Aviation Accident Summaries

Aviation Accident Summary DFW06LA198

Parkdale, AR, USA

Aircraft #1

N444HF

Ayres S2R-T34

Analysis

The 6,000-hour commercial pilot made a forced landing to a cotton field after the turbine engine installed on his agricultural airplane stopped producing power. The pilot landed in a field and subsequently collided with trees. An inspector with the Federal Aviation Administration performed an on-scene examination of the airplane. According to the inspector, the airplane sustained structural damage to the wings. Examination of the engine revealed a compressor-turbine blade had failed causing extensive damage to the vein ring, segments and small exit duct. This failure also resulted in debris contacting the power-turbine blades, which subsequently damaged all of the power-turbine blades and disc. The failed blade was never located and the mode of failure could not be determined. A review of the airplane's maintenance history revealed that the compressor-turbine disc was rebladed in November 1994, and had accumulated approximately 4,987.7 hours since new. The disc itself had accumulated approximately 7,941.4 hours and 7,170 cycles.

Factual Information

On August 11, 2006, at 1130 central daylight time, a single-engine Ayres S2R-T34 agricultural airplane, N444HF, was substantially damaged during a forced landing following a reported loss of engine power while maneuvering near Parkdale, Arkansas. The commercial pilot, sole occupant of the airplane, was not injured. The airplane was registered to McGinty Flying Service, of Jones, Louisiana, and was being operated by Wilmot Aero of Parkdale, Arkansas. Visual meteorological conditions prevailed and no flight plan was filed for the local aerial application flight conducted under 14 Code of Federal Regulations Part 137. A Federal Aviation Administration (FAA) inspector performed an on-scene examination of the airplane. According to the inspector, the pilot reported that the engine suddenly stopped producing power and he executed a forced landing in a cotton field. The airplane sustained structural damage to the right wing and outboard section of the left wing. Examination of the turbine engine revealed a compressor-turbine blade, Part number T-102401-792A, had failed causing extensive damage to the vein ring, segments and small exit duct. This failure also resulted in debris contacting the power-turbine blades, which subsequently damaged all of the power-turbine blades and disc. Additional damage was noted on the exhaust duct and power-turbine shroud. The failed blade was never located and the mode of failure could not be determined. A review of the airplane's maintenance records revealed that the compressor-turbine disc was last rebladed in November 1994, and had accumulated approximately 4,987.7 hours. The disc itself had accumulated approximately 7,941.4 hours and 7,170 cycles. The pilot's last FAA second class medical was issued on January 4, 2006. At that time, the pilot reported having accumulated a total of 6,000 flight hours. The pilot did not submit a completed Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) as of the time this factual report was released. Weather at the Mid-Delta Regional Airport, near Greenville, Mississippi, at 1053, was reported as wind from 330 degrees at 6 knots, clear skies, temperature 91 degrees Fahrenheit, dewpoint 71 degrees Fahrenheit, and a barometric pressure setting of 29.92 inches of Mercury.

Probable Cause and Findings

The failure of a compressor turbine blade for undetermined reasons, which resulted in a total loss of engine power. A contributing factor was the lack of suitable terrain for the forced landing.

 

Source: NTSB Aviation Accident Database

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