Aviation Accident Summaries

Aviation Accident Summary ANC07LA008

Anchorage, AK, USA

Aircraft #1

N752SA

Boeing 747-228F

Analysis

The flight crew departed on an instrument flight rules (IFR) non-scheduled domestic cargo flight under Title 14, CFR Part 121. When the cabin failed to pressurize during departure, the airplane returned to the airport. An FAA inspector who examined the airplane reported that maintenance personnel found a penetrating gouge in the right lower portion of the fuselage between the wing and tail, near the cargo door. The inspector indicated that the gouge was 18 inches long, 1 to 2 inches wide, with other, shallower surface skin damage about 3 feet long, and that the damage was consistent with the size and shape of the counter-balance weight on the truck used to deice the airplane.

Factual Information

On December 23, 2006, about 2145 Alaska standard time, a Boeing 747-228F airplane, N752SA, sustained substantial damage when it was struck by a deicing truck during deicing at the Ted Stevens Anchorage International Airport, Anchorage, Alaska. The flight crew was aboard preparing the airplane for flight. The airplane was being operated as Flight 996, by Southern Air Inc., Norwalk, Connecticut, as an instrument flight rules (IFR) non-scheduled domestic cargo flight under Title 14, CFR Part 121, when the accident occurred. The three flight crew members were not injured. Instrument meteorological conditions prevailed, and an instrument flight plan was filed. The airplane departed Anchorage about 0030, and was bound for Dallas, Texas, but returned when the crew was unable to pressurize the cabin. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) on December 26, the FAA inspector who examined the airplane, reported that after the airplane departed Anchorage, the flight crew discovered that the cabin would not pressurize, and they returned to Anchorage and landed. The inspector said during an inspection of the airplane, maintenance personnel found a penetrating gouge in the right lower portion of the fuselage between the wing and tail, near the cargo door. The inspector indicated that the penetrating gouge was 18 inches long, 1 to 2 inches wide, with other, shallower surface skin damage about 3 feet long. He said the damage was consistent with the size and shape of the counter-balance weight on the truck used to deice the airplane.

Probable Cause and Findings

The failure of the deicing truck crew to maintain sufficient distance from the parked airplane during deicing, which resulted in a collision and substantial damage to the airplane.

 

Source: NTSB Aviation Accident Database

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