Aviation Accident Summaries

Aviation Accident Summary CHI07FA107

Lake Michigan, MI, USA

Aircraft #1

N77181

Canadair CL-600-2B19

Analysis

The flight crew received a left thrust reverser unlock indication while holding for takeoff. The captain cycled the reverser, and had decided to return to the gate when the messages cleared. With the issue apparently resolved, he elected to takeoff. The captain reported experiencing a small vibration on climb out and, a short time later, he heard a "loud bang" and the "aircraft pitched and yawed/rolled to [the] left." The autopilot disengaged and the left thrust lever moved to idle during the event. The first officer ran the checklist to stow the reverser. The captain decided to continue to the intended destination because the thrust reverser messages had cleared and the vibrations had stopped. The flight subsequently landed uneventfully. The flight data recorder (FDR) indicated that the left engine vibration levels were elevated during the accident flight. Approximately 3 minutes into the flight, the left engine thrust reverser unlocked parameter changed to "On" for about 1 second. About 11:20 (MM:SS) after takeoff, the left engine vibration level increased momentarily, and both the left and right engine speeds and fuel flows began to decrease. As the decrease in fuel flows was occurring, the airplane rolled right, left, and right again over about a 4-second period. The decrease in engine parameters lasted over 3 minutes before returning to normal. The left engine thrust reverser unlock parameter indicated "On" for about 4 seconds during that time. The left engine vibration levels decreased after the event, below the levels previously recorded during the flight, and approximately to the level of the right engine vibration. The vibration and engine speed variations suggested separation of the left engine translating cowling at that point. The left engine thrust reverser deploy parameter remained in the "Off" state for the entire flight. Additionally, the FDR data revealed that the left engine vibration levels were elevated and left engine thrust reverser did not deploy on the two previous flights. The post accident inspection revealed that the left engine translating cowl had separated from the engine assembly and damaged the empennage. Damage to the thrust reverser components was consistent with prior operation with the reverser out of alignment and jamming of the translating structure. Review of the aircraft's maintenance records revealed a history of anomalies related to the left engine thrust reverser. About one month prior to the accident, the aircraft maintenance log contained the discrepancy, "L Rev Unlock Caution." The entry was deferred in accordance with the minimum equipment list (MEL). The left pneumatic drive unit and the left thrust reverser flex shafts were subsequently replaced; however the discrepancy was not resolved. Eleven days after the initial write-up, a ballscrew actuator and a cascade assembly were replaced. The maintenance record indicated that rigging and operational checks were satisfactory, and the MEL item was closed. There were no further entries related to the left thrust reverser in the aircraft maintenance log. The MEL allowed the airplane to be dispatched with one of the engine thrust reversers inoperative. It required that the inoperative reverser be inspected for structural damage, deactivated, and stowed and locked in the forward thrust position. In the event of an in-flight unlock or deploy indication, the flight manual instructed the crew to manually stow the reverser. There was no guidance in the event of an indication on the ground. Bombardier has initiated a revision to the flight manual to include instructions in the event of a thrust reverser unlock message received during ground operations.

Factual Information

HISTORY OF FLIGHT On April 7, 2007, about 2123 eastern daylight time, a Canadair CL-600-2B19 (CRJ), N77181, operated by Mesa Airlines as flight 7264, was substantially damaged when the thrust reverser translating cowling separated from the left engine during cruise flight and struck the horizontal and vertical stabilizers. The airplane was near the eastern shore of Lake Michigan, about 35 miles west-northwest of Grand Rapids, Michigan, when the accident occurred. The revenue air carrier flight was operating under 14 CFR Part 121 on an instrument flight rules (IFR) flight plan. Visual meteorological conditions prevailed in the vicinity at the time of the accident. The one passenger, one flight attendant, and two pilots on-board were not injured. The flight departed Capital City Airport (LAN), Lansing, Michigan, at 2054. The flight continued to the intended destination, Chicago O'Hare International Airport (ORD), Chicago, Illinois, and landed without further incident at 2136. The captain noted that air traffic into ORD was under flow restrictions and the flight had to wait for its assigned release time. While holding for takeoff at LAN, the flight crew received a left thrust reverser unlock master caution and associated Engine Indicating and Crew Alert System (EICAS) indications. The captain contacted maintenance and cycled the reverser a few times in an attempt to clear the indications. He had decided to return to the gate when the messages cleared. He subsequently cycled the thrust reversers two or three more times and both appeared to be operating and stowing properly. Since the thrust reversers seemed to be operating normally, he elected to depart for ORD. The captain reported experiencing a small vibration on climb out. The flight climbed to a cruise altitude of 16,000 feet mean sea level. The vibration persisted and the captain became concerned about the thrust reverser. He stated that about 35 miles west-northwest of Grand Rapids, he heard a "loud bang" and the "aircraft pitched and yawed/rolled to [the] left." The autopilot disengaged and the left thrust lever moved to idle during the event. The first officer ran the checklist to stow the reverser. The captain hand flew the airplane for a time. He ultimately elected to continue to ORD because the thrust reverser unlock messages had cleared and the vibrations had stopped. The flight subsequently landed uneventfully at ORD. The autopilot and trim system worked properly after the event. The missing left engine cowling and damage to the empennage were observed during the post flight inspection. PERSONNEL INFORMATION The pilot-in-command (captain) held an Airline Transport Pilot certificate with multi-engine and single-engine airplane ratings. His certificate included CL-65 and EMB-145 type ratings. He was issued a First Class Airman Medical Certificate without limitations or waivers on December 8, 2006. He had accumulated approximately 8,000 hours total flight time, with about 500 hours in CRJ aircraft. His most recent flight check was completed on February 22, 2007. The second-in-command (first officer) held an Airline Transport Pilot certificate with multi-engine and single-engine airplane ratings. The single-engine rating was limited to commercial pilot privileges only. His certificate included a CL-65 type rating limited to second-in-command privileges only. He was issued a First-Class Airman Medical Certificate without limitations or waivers on December 8, 2006. He had accumulated approximately 5,600 hours total flight time, with about 2,920 hours in CRJ aircraft. His most recent flight check was completed on January 13, 2007. AIRCRAFT INFORMATION The accident airplane was a 1997 Canadair (Bombardier) CL-600-2B19, serial number 7181. It was certificated as a transport category airplane under Type Certificate A21EA. It was configured with 50 passenger seats. The airplane was powered by two General Electric CF34-3B1 turbofan engines, rated at 9,300 lbs. of thrust. At the time of the accident, the airplane had accumulated 24,805 hours flight time. The left engine, serial number GE-E872898, had accumulated 11,489 hours time in service. The right engine, serial number GE-E872265, had accumulated 22,856 hours time in service. Review of the aircraft's maintenance records revealed a history of anomalies related to the left engine thrust reverser. On March 11, 2007, the aircraft maintenance log contained the discrepancy, "L Rev Unlock Caution." The entry was deferred in accordance with the Mesa Airlines CRJ Minimum Equipment List (MEL). On March 18, 2007, the left pneumatic drive unit was replaced; however, operational testing determined that the discrepancy was not resolved. The maintenance record noted binding in the drive assembly to the ballscrew actuator. On March 20, 2007, the left engine thrust reverser flex shafts were replaced. Again, the discrepancy was not resolved. On March 22, 2007, a ballscrew actuator and a cascade assembly were replaced. The maintenance record indicated that rigging and operational checks were satisfactory. The MEL item was closed at that time. Routine maintenance was conducted on March 30, 2007, at which time the thrust reverser and ballscrew actuators were lubricated. No defects were noted in the records. Subsequent to the date the MEL was closed, there were no entries related to the left thrust reverser in the aircraft maintenance log. The flight log indicated that on the day of the accident, the airplane flew from Columbia Metropolitan Airport (CAE), Columbia, South Carolina, to ORD. The airplane then flew to Harrisburg International Airport (MDT), Harrisburg, Pennsylvania, and back to ORD. The next flight, which was the flight prior to the accident flight, was from ORD to LAN. According to the log, that flight landed at 1943. The Mesa Airlines CRJ MEL, dated July 14, 2006, stated that an airplane may be dispatched with one of the engine thrust reversers inoperative. The MEL required that the inoperative reverser be inspected for structural damage, deactivated, and stowed and locked in the forward thrust position. METEOROLOGICAL INFORMATION Surface weather conditions recorded at the Gerald R. Ford Airport (GRR), Grand Rapids, Michigan, at 2056, were: Winds from 280 degrees at 9 knots; 10 miles visibility; broken clouds at 5,500 feet above ground level (agl); overcast clouds at 7,500 feet agl; temperature and dew point -03 and -07 degrees Celsius, respectively; altimeter 29.93 inches of mercury. FLIGHT RECORDERS The NTSB Vehicle Recorders Laboratory downloaded the flight data recorder (FDR) and the data were reviewed. Elapsed time is noted in minutes and seconds (MM:SS) relative to the airplane becoming fully airborne (weight-off-wheels signals from all three landing gear). The data indicated that: At 03:14 (MM:SS) after liftoff, as the airplane climbed through approximately 8,500 feet pressure altitude, the left engine thrust reverser unlock parameter indicated "On" for about one second. At 05:42 into the flight, the left engine fuel flow began to decrease, followed by the engine speed (N1 and N2 parameters). The fuel flow decreased over a period of approximately 20 seconds before returning to the previous level. The engine speed followed that trend. At 11:20, both engine fuel flows and engine speeds again began to decrease. Just prior to this, the left engine vibration parameter increased for approximately 2 seconds, before dropping below the left engine vibration level recorded earlier in the flight. As this fuel flow decrease was occurring, the airplane rolled right, left, and right again over about a 4-second period. The decrease in the left engine parameters lasted over 3 minutes. The decrease in the right engine parameters lasted for approximately 2 minutes before both began to increase again to normal levels. At 14:46, the left engine thrust reverser unlocked parameter again indicated "On" for 4 seconds. It remained "Off" for the remainder of the flight. This occurred about the time the engine parameters returned to normal. At 32:12, while the airplane was descending, the left engine thrust reverser arm advisory indicated "On" and remained in that state for the remainder of the flight. The left engine thrust reverser deploy parameter remained in the "Off" state for the entire flight. The right engine reverser deploy parameter indicated "On" for approximately 9 seconds during landing. This was concurrent with the right engine thrust reverser unlocked parameter indicating "On" for about 13 seconds during the landing. The FDR data related to the two flights prior to the accident flight indicated that the left engine thrust reverser did not deploy properly. On the flight prior to the accident flight, during landing, both the left and right engine thrust reverser unlocked parameters indicated "On" for approximately 20 seconds. However, the left engine thrust reverser deployed parameter remained "Off" during that time period. The right engine thrust reverser deployed parameter indicated "On" for about 15 seconds during that time. During landing on the second flight prior to the accident flight, the left and right thrust reverser unlocked parameters went from "Off" to "On" within about 1 second of each other. The left engine reverser unlocked parameter remained "On" for approximately 13 seconds. It went to "Off" for 9 seconds, and then indicated "On" again briefly for 1 second and again for 3 seconds, before remaining "Off" for the remainder of the flight. During that time, the left engine thrust reverser deployed parameter indicated "Off" for the entire time. The right engine thrust reverser unlocked parameter indicated "On" for approximately 22 seconds. It then switched to "Off" and remained in that state for the remainder of the flight. The right engine thrust reverser deployed parameter indicated "On" beginning about 3 seconds after the reverser unlocked parameter went to "On." The reverser deployed parameter remained on for about 16 seconds. It subsequently went to "Off" and remained in that state for the remainder of the flight. The aircraft maintenance log did not contain any entries related to any left engine thrust reverser malfunctions during these flights. WRECKAGE AND IMPACT INFORMATION A post accident inspection revealed that the left engine translating cowl had separated from the aircraft. The inboard leading edge of the left horizontal stabilizer was dented and crushed aft consistent with impact damage. The left side skin of the vertical stabilizer was punctured immediately forward of the center spar. The puncture was approximately 8 inches long by 2 inches wide, oriented vertically parallel to the spar. The engine and available thrust reverser components were examined. The translating cowl was not recovered. A portion of the lower translating cowling hinge remained attached to the track. Two translating cowling interlock fittings had separated from the assembly. The fittings remained secured to the torque box at the latch fittings with the shoot bolts engaged. The upper thrust reverser pylon attachment track exhibited scoring along the Auto Throttle Retard (ATR) cam. The track was bowed approximately 3/8 inch in an area about 9 inches from the aft end of the component. No anomalies associated with the lower attachment track were observed. One torque box interlock fitting was fractured and missing. The remaining five interlock fittings were intact. The torque box itself was twisted, and the outer skin and rear bulkhead were creased. The upper inboard actuator clevis end attachment pin was sheared. The jackscrew mechanism rotated without binding. TESTS AND RESEARCH The left engine thrust reverser Pneumatic Drive Actuator (Part number 126785-7 / Serial number 2240) was tested by the component manufacturer under direct supervision of the Federal Aviation Administration. No anomalies consistent with an in-flight un-commanded thrust reverser deployment were observed. The thrust reverser deployment lockout mechanism appeared undamaged. ADDITIONAL INFORMATION The Mesa Airlines CRJ Company Flight Manual, dated December 12, 2007, specified that in the case of a left or right reverser unlock message (L/R REV UNLOCKED), the flight crew is to confirm that the affected thrust lever is at idle, and to select the corresponding Thrust Reverser Emergency Stow switch. According to the manual, "improved airplane handling and normal operation of [the] affected thrust lever," indicated successful stowage of the thrust reverser. An Auto Throttle Retard (ATR) System is designed to insure that the throttle lever is at idle whenever the thrust reverser is in transit. In flight, if a thrust reverser is inadvertently deployed, the affected throttle lever is automatically retarded to idle to minimize asymmetric thrust. An ATR commanded thrust reduction normally occurs in less than one second. According to the Federal Aviation Administration and Bombardier, this event is the only known CRJ-100/200 in-flight translating cowl separation. Bombardier revised the flight manual to include detailed instructions in the event that a left or right reverser unlock message (L or R REV UNLOCKED) is received during ground operations.

Probable Cause and Findings

In-flight separation of the left engine thrust reverser translating cowling due to intermittent binding and jamming of the reverser on the accident flight and on previous flights. Contributing factors were the inadequate maintenance action by the operator due to their failure to properly resolve the prior reverser malfunctions, the failure of the pilots of previous flights in not referring earlier reverser deployment failures for maintenance action, and incomplete company/manufacturer's procedures because they did not address anomalous reverser indications during ground operations.

 

Source: NTSB Aviation Accident Database

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