Aviation Accident Summaries

Aviation Accident Summary NYC07LA168

E.Stroudsburg, PA, USA

Aircraft #1

N7389J

PIPER PA-28-140

Analysis

The pilot of a Piper PA-28-140 was returning to his original departure airport after conducting stop-and-go landings at two other airports. Another pilot, who entered the traffic pattern at the same time as the accident pilot, heard the accident pilot transmit that he was turning on to the left base leg of the traffic pattern for the active runway. No further transmissions were heard from the accident airplane. The airplane was observed moments before the accident to be just above the top of trees before passing over a house while turning to the left. It then sounded like the "engine turned off." The sound of a thump was then heard. A resident ventured into the woods, and discovered the wreckage of the airplane. She did not smell any gasoline and discovered the pilot lying near the fuselage. Post accident examination of the airplane revealed no evidence of any preimpact malfunction of the airplane or engine. The propeller exhibited signatures consistent with a low rpm (windmilling) event. The left wing was separated from its attachment fittings and was found leading edge down leaning against a tree. One to two gallons of fuel were discovered in the forward portion of the tank. The right wing's fuel tank was breached and void of fuel. No fuel staining was observed on the ground surrounding the tank, and no smell of fuel was detected on site. The fuel selector was found in the left tank position.

Factual Information

HISTORY OF FLIGHT On July 15, 2007, about 2250 eastern daylight time, a Piper PA-28-140, N7389J, was substantially damaged when it impacted trees near Stroudsburg-Pocono Airport (N53), East Stroudsburg, Pennsylvania. The certificated private pilot was seriously injured. Night visual meteorological conditions prevailed and no flight plan was filed for the personal flight conducted under 14 Code of Federal Regulations Part 91. According to the pilot, he was returning to N53 after conducting stop and go landings at two other airports in order to meet the night aeronautical experience requirements for a commercial pilot certificate. He could not however, remember the circumstances surrounding the accident with the exception of "hitting the trees." According to Federal Aviation Administration (FAA), air traffic control facility records the airplane departed N53 and performed stop and go landings at Wilkes-Barre/Scranton International Airport (AVP), Scranton, Pennsylvania and Lehigh Valley International Airport (ABE), Allentown, Pennsylvania before returning to N53. According to another pilot, who entered the traffic pattern the same time the accident pilot did on his return to N53, the accident pilot transmitted that he was turning on to the left base leg of the traffic pattern for runway 8. No further transmissions were heard. A witness, who observed the airplane moments before the accident, stated that the airplane was "just above the trees" before it passed over his house turning to the left. It then sounded like the "engine turned off and it crashed." Another witness reported that she heard a "thump," and looked out the window of her house, but could not see anything. Approximately 10-minutes later she heard a helicopter and saw searchlights. After instructing her husband to call "911," she ventured approximately 300 feet into the woods, and discovered the wreckage of the airplane. The airplane’s interior lights were still illuminated, and she discovered the pilot lying near the fuselage. She did not smell any gasoline and believed there was no danger of fire so she did not attempt to move him away from the wreckage. PERSONNEL INFORMATION According to FAA records, the pilot held a private pilot certificate, with ratings, for airplane single-engine land, and instrument airplane. He reported a total flight experience of 520 hours. His most recent FAA second-class medical certificate was issued on December 22, 2006. AIRCRAFT INFORMATION According to FAA and maintenance records, the airplane was manufactured in 1968. The airplane's most recent annual inspection was completed on December 15, 2006. At the time of the inspection, the airplane had accrued 4,734.57 total hours of operation. METEOROLOGICAL INFORMATION A weather observation taken 3 minutes after the accident, at Pocono Mountains Municipal Airport (MPO), Mount Pocono, Pennsylvania, located approximately 12 nautical miles northwest of the accident site, included: variable winds at 3 knots, visibility 10 miles, scattered clouds at 9,000 feet, overcast ceiling at 12,000 feet, temperature 22 degrees Celsius, dew point 16 degrees Celsius, and an altimeter setting of 29.92 inches of mercury. WRECKAGE AND IMPACT INFORMATION No evidence of any preimpact malfunction of the airplane or engine was discovered. Examination of the accident site and wreckage by an FAA inspector revealed, that the airplane had come to rest on its left side. The left wing had separated from its attachment fittings and was found leading edge down leaning against a tree. Approximately 6 inches of fuel was discovered in the forward portion of the tank. The right wing remained attached at its fittings, and its fuel tank was breached. It was void of fuel. No fuel staining was observed on the ground surrounding the tank, and no smell of fuel was detected on site. The fuel selector was in the left tank position. The Flap extension handle was in the 40-degree position. Control continuity was confirmed from the stabilator, rudder, and right aileron to the pitch, yaw and roll control mechanisms in the cabin. Control continuity for the left aileron was confirmed to the breaks in the actuating cables, which exhibited evidence of tensile overload and corresponded to the point of separation of the wing at the wing root. Examination of the engine revealed, that the engine was still attached to its mounts and the firewall. The cowling was crumpled but remained in place. The propeller and spinner were also in place and remained attached to the engine. Both propeller blade tips were bent and had large nicks in them. One blade had chordwise scratches across most of the leading edge. Neither blade displayed significant bending or twisting. The engine was found to have incurred impact damage to the No. 2 cylinder head area. The top spark plug was broken away, and the helicoil threads from the cylinder were pulled out. The bottom spark plug remained in place, however the ignition lead was separated. The top left area of the cylinder head where the rocker box cover attached was also broken away. The intake pushrod housing was crushed. The intake tube was in place and crushed. The oil return line and primer line had separated and were also crushed. The exhaust system was damaged, and both ends had separated from the muffler. All cylinders were inspected with a lighted borescope and no discrepancies were noted. The engine drive train was rotated through the vacuum pump accessory drive and was found to rotate freely and completely in both directions. Continuity was confirmed to all rocker arms and aft gears. Thumb compression was confirmed on all cylinders. Magneto to engine timing was confirmed and during rotation of the drive train, the left magneto impulse coupling could be heard to click. Spark was confirmed from all leads to the left magneto. The right magneto was rotated by hand. It also produced spark at all ignition leads. TESTS AND RESEARCH According to a witness, the airplane had already been flown by the pilot earlier in the day. A query of fuel providers at surrounding airports revealed that the airplane had been refueled sometime prior to 1440 on the day of the accident at ABE and that the fuel tanks had been filled to maximum capacity at that time.

Probable Cause and Findings

The pilot's improper fuel management resulting in loss of engine power.

 

Source: NTSB Aviation Accident Database

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