Aviation Accident Summaries

Aviation Accident Summary LAX08LA240

Bountiful, UT, USA

Aircraft #1

N7672

CESSNA 172M

Analysis

During takeoff initial climb at an altitude of about 100 feet above ground level, the climb performance of the airplane degraded along with a partial loss of engine power. The certified flight instructor (CFI) advanced the mixture to the full rich position, checked the carburetor heat, and verified that the throttle was full forward. The CFI then took control of the airplane from the student pilot, and initiated a forced landing into an open soft field. During the landing, the wheels of the airplane sunk into mud, and the airplane nosed over. Examination of the engine, fuel system, and airframe systems related to engine operation revealed no anomalies that would have precluded normal operation.

Factual Information

On July 22, 2008, about 1725 mountain daylight time, a Cessna 172M single-engine airplane, N7672, made a forced landing following a partial loss of engine power during takeoff initial climb from the Skypark Airport (BTF), Bountiful, Utah. The airplane was registered to a private individual, and operated by G&B Aircraft Management, Woods Cross, Utah, under the provisions of Title 14 Code of Federal Regulations Part 91. The certified flight instructor (CFI) and student pilot received minor injuries; the airplane sustained substantial damage to the fuselage and left wing. Visual meteorological conditions prevailed, and no flight plan was filed for the instructional flight. The local flight was originating at the time of the accident. The CFI reported that the accident flight was the first flight of the day for the airplane. Prior to takeoff, the student pilot "leaned the mixture for altitude" during a normal engine run up. The student taxied to the active runway, and proceeded to takeoff. As the airplane climbed through about 100 feet above ground level (agl), the airplane's climb performance degraded along with a partial loss of engine power. The CFI advanced the mixture to full rich, checked the carburetor heat, and verified that the throttle was full forward, but noticed no increase in the climb rate. The CFI then took control of the airplane, and initiated a forced landing to an open field beyond the departure end of the runway. During the landing roll, the wheels of the airplane sunk into mud, and the airplane nosed over. Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that the airplane came to rest inverted within an open field about 1/4 mile north of BTF. Both left and right wing fuel tanks were full of 100-low lead aviation fuel. Examination of the Lycoming O-320-E2D engine, serial number L-22287-27A, by an NTSB investigator revealed no anomalies that would have precluded normal operation and production of power. No anomalies were noted with the airframe fuel system.

Probable Cause and Findings

A partial loss of engine power for undetermined reasons.

 

Source: NTSB Aviation Accident Database

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