Aviation Accident Summaries

Aviation Accident Summary LAX08CA207

Fullerton, CA, USA

Aircraft #1

N1296M

Cessna T206H

Analysis

The pilot was conducting a normal approach to landing and reported that he maintained proper airspeed and alignment to the runway. The airplane was centered and nose-high as the main gear touched down. The pilot said the airplane suddenly tipped to the left, the propeller struck the runway, and then the right wing tip contacted the runway surface. The airplane came to rest at the center of the runway. The airplane sustained substantial damage to the firewall and left wing spar. Inspection of the airplane under the supervision of the Federal Aviation Administration revealed no discrepancies with the rudder and brake systems and control system components. The rudder and aileron trim positions were neutral, and there was a difference of about 2 gallons of fuel between the wing tanks. Inspectors also found that the main landing gear wheel fairings were properly installed with no anomalies.

Factual Information

In a written report, the pilot stated that he was conducting a normal approach to landing on runway 24. He stated that the airplane's speed was fine, and that he was straight on the final approach. He noted that the airplane landed with the nose of the airplane up and directly over the runway centerline. As the main gear touched down on the runway, the airplane tipped to the left, the propeller struck the runway, and then the right wing tip contacted the runway surface. The pilot reported that the airplane came to rest near the center of the runway. Later inspection of the airplane revealed substantial damage to the firewall and left wing spar. An aviation routine weather report (METAR) for Fullerton Municipal Airport (KFUL) was issued at 1653 PDT, about 7 minutes before the accident. It stated: winds from 230 degrees at 5 knots; visibility 8 miles; skies clear; temperature 23 degrees Celsius; dew point 13 degrees Celsius; altimeter 29.90 inches of mercury. Under the supervision of the Federal Aviation Administration (FAA), maintenance personnel at Fullerton inspected the airplane. Inspection of the brake system operation revealed no discrepancies. Rudder operation and travel were normal, with or without the parking brake on. The trim setting for both the ailerons and the rudder were found in a near-neutral position. Inspectors drained both wing tanks, and found a difference of about 2 gallons of fuel between the two tanks. A second inspection of the airplane included the main landing gear wheel fairings. No anomalies were noted, and inspectors confirmed proper installation of the parts. The inspectors observed that the right brake assembly and operation had no discrepancies. The FAA inspectors also noted that the airplane was recently purchased new, and had a total time of 60.2 hours.

Probable Cause and Findings

The pilot's failure to maintain control of the airplane during the landing touchdown, resulting in the wings contacting the runway surface and a propeller strike.

 

Source: NTSB Aviation Accident Database

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