Aviation Accident Summaries

Aviation Accident Summary SEA08CA184

Moses Lake, WA, USA

Aircraft #1

N2505Q

Wheat Excalibur EX

Analysis

The pilot was on a local, personal flight in an experimental airplane. While in cruise flight approximately 600 feet above ground level he heard a loud bang and the airplane entered a right turn. The pilot used aileron to counteract the turn; however, the airplane descended into the reservoir below. Post accident inspection showed that the rivets securing the rudder pedals had sheared in overload and there was no evidence of corrosion. During the impact sequence, the fuselage sustained structural damage. According to the kit supplier, the rudder pedal horns are secured using three rivets per pedal. The kit supplier indicated that the rivets could be put under excessive stress while operating the airplane over gross weight and/or powering the airplane with an engine that produces over 65 horsepower. The engine installed in the airframe produced 85 horsepower. As a result of the accident, the kit supplier suggested that the builders include a rudder pedal security check and if they are loose, replace two of the three rivets with two bolts. All future designs kits produced and shipped will include the bolts.

Factual Information

The pilot was on a local, personal flight in an experimental airplane that had accumulated 32 hours total time. It was powered by an engine that produced 85 horsepower. While in cruise flight approximately 600 feet above ground level he heard a loud bang and the airplane entered a right turn. The pilot used aileron to counteract the turn; however, the airplane descended into the reservoir below. Post accident inspection showed that the rivets securing the rudder pedals had sheared. During the impact sequence, the fuselage sustained structural damage. According to the kit supplier, the rudder pedal horns are secured using three rivets per pedal. The kit supplier indicated that the rivets could be put under excessive stress while operating the airplane over gross weight and/or powering the airplane with an engine that produces over 65 horsepower. Although there had been no other reports of this kind to the kit supplier, following the accident he suggested to his customers that they check the security of the rivets prior to each flight and if they are loose, replace two of the three rivets with two bolts provided by the kit supplier. All future rudder pedals provided by the kit supplier will be equipped with the bolts.

Probable Cause and Findings

The right rudder pedal attach rivets sheared due to overload.

 

Source: NTSB Aviation Accident Database

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