Aviation Accident Summaries

Aviation Accident Summary ERA12IA090

Nantucket, MA, USA

Aircraft #1

N303PJ

CESSNA 402B

Analysis

The multi-engine airplane was approaching the destination airport with about 7 gallons of fuel remaining in each of the 50-gallon left and right main fuel tanks. While on short final approach to land, as the pilot fully extended the flaps, the airplane experienced a total loss of power on the right engine. The airplane touched down hard on a grassy area about 650 feet before the runway, bounced onto the runway, and came to rest. The pilot subsequently started both engines and taxied to the ramp area uneventfully. A postaccident examination of the airplane revealed that the right main fuel tank fuel transfer pump was inoperative. The fuel transfer pump was designed to operate continuously when the battery switch was in the on position. The purpose of the fuel transfer pump was to transfer fuel from the nose section of its respective main fuel tank to the fuel pick-up area near the center of the main fuel tank, which permitted steep descents with low main tank fuel quantity. It could not be determined when the fuel transfer pump failed; however, confirming pump operations was a required preflight inspection item for each main fuel tank.

Factual Information

On November 29, 2011, at 1333 eastern standard time, a Cessna 402B, N303PJ, operated by Nantucket Express, incurred minor damage while landing at Nantucket Memorial Airport (ACK), Nantucket Massachusetts. The certificated airline transport pilot was not injured. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the flight that departed Norwood Memorial Airport (OWD), Norwood, Massachusetts, about 1300. The pilot reported that he was returning home, following a flight evaluation. While on a short final approach to runway 15, as he fully extended the flaps, the left engine experienced a total loss of power. The pilot switched fuel tanks for the left engine; however, it did not restart and the airplane descended quickly. The airplane touched down on a grassy area about 650 feet prior to the runway. It then bounced onto the runway and came to rest. During the landing, the right propeller and left wing skin were damaged. The pilot subsequently started both engines and taxied to the ramp area uneventfully. Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that there was approximately 7 gallons of fuel in the left main fuel tank. There was also about 7 gallons of fuel in the right main fuel tank and approximately 2 gallons of fuel in each auxiliary fuel tank. The fuel was sampled and no contamination was noted. Additionally, an examination of the left engine did not reveal any mechanical malfunctions. The FAA inspector reported that the 50-gallon left and right main fuel tanks were each equipped with a fuel transfer pump, which pumped fuel from the front of its respective main fuel tank to the fuel pick-up near the center of the main fuel tank. The fuel transfer pumps were designed to operate continuously whenever the airplane battery switch was in the on position. During examination of the airplane, the FAA inspector noted that the left main fuel tank transfer pump was operating and the right main fuel tank transfer pump was not. During a telephone interview following the airplane examination, the pilot stated that the incident happened so fast and on such a short final approach, that he could not be certain which engine lost power. He added that it was quite possible the right engine experienced the loss of power. The pilot further stated that he moved the left engine fuel selector from left main to left auxiliary as he believed he had a left engine failure. Review of a pilot's operating handbook (POH) for the make and model airplane, section 4, Preflight Inspection, revealed, in part, "…Battery Switch – ON…Tip Tank Transfer Pump – LISTEN for operation…" with regards to the left and right main (tip) fuel tanks. Further review of the POH, section 7, Airplane and System Descriptions, revealed, in part, "…The transfer pump, mounted on the aft side of the main tank rear bulkhead, transfers fuel from the nose section of the main tank to the center sump area, where it is picked up and routed to the engine by the engine-driven or auxiliary fuel pump. The transfer pump permits steep descents with low main tank fuel quantity…" Review of FAA service difficulty reports for the make and model airplane revealed one other report of a fuel transfer pump failure.

Probable Cause and Findings

The failure of the right main fuel tank transfer pump, which resulted in a total loss of engine power on the right engine during approach due to fuel starvation, and a subsequent hard landing. Contributing to the incident was the pilot's operation of the airplane with a low fuel quantity.

 

Source: NTSB Aviation Accident Database

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